seminar58 castro presentation_3

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CITE CITE- AHU: AHU: An Automated Commissioning Tool for CAV An Automated Commissioning Tool for CAV Air Air- Handling Units Handling Units Natascha Castro, NIST Natascha Castro, NIST Hossein Hossein Vaezi Vaezi- Nejad Nejad, CSTB , CSTB IEA Annex 40

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Page 1: Seminar58 castro presentation_3

CITECITE--AHU: AHU: An Automated Commissioning Tool for CAV An Automated Commissioning Tool for CAV AirAir--Handling UnitsHandling Units

Natascha Castro, NISTNatascha Castro, NISTHossein Hossein VaeziVaezi--NejadNejad, CSTB, CSTB

IEA Annex 40

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Outline

n Commissioning Processn Development of CITE-AHU¨ Test automation¨ Expert rules¨ Interface

n Commissioning the ARIA Building¨ Design Review¨ Manual Cx Results¨ Automated Cx Results

n Savings Estimate/ Paybackn Conclusions

CITE-AHU Commissioning of the Installation and Technical Equipment-Air Handling Units

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Step 1: Design Review-check control logic, sensor placement and sensor accuracy.

Step 2: Operator Interview-for existing buildings, ask building operator whether the air handling units are operating properly to the best of their knowledge.

Step 3: Installation Review and Verification-conduct a field inspection to determine installed characteristics of the equipment including condition and sensor availability

Step 4: Forced Response Testing and Analysis-

manipulate the system under test by means of setpoint changes and sensor overrides. Document along with mode changes. Evaluate data for compliance.

MANUAL

BEMS

AHU AHU CommissioningCommissioning ProcessProcess ((fromfrom CTPL)CTPL)

not currently emphasized in protocols

iterative!

complete passive testing with BEMS, before active testing

update documents

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1. Verify communications link2. Run pre-coded test sequence from library

Value Displays as READ is completed

This is the line number to input to change reference value

Automation of functional test scripts

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1. Import test data 2. Specify data relationships3. Specify system functionality4. Analyze using modified APAR rules5. Compare to archived tests for On-going Cx

CAV

VAV

ProcedureProcedure for Cx for Cx AnalysisAnalysis

CITE-AHU

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• Enhanced for constant air volume systems

CITE-AHU

Provides greater transparency of rule logic (tool tips )

CITE-AHU

Expert rules- AHU Performance Assessment Rules (House)

• Considers additional equipment (heat recovery)

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Commissioning the ARIA Building

¨ Design Review¨Manual Cx¨ Automated Cx

n Serves Offices & Converted space

n 100% outdoor air

n Modes:

¨ Heating

¨ Free cooling

w/ Heat recovery & Manual Bypass

Step 1 Design Review: AHU3

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n Candid w/ good knowledge of (undocumented) system history.

Cannot change the controllers schedule, setpoints revert to a nightly shutoff at midnight and 05:00 startup

General

Zones partitioned for office spaces w/o changing ventilation configuration

AHU3

PROBLEM DESCRIPTION UNIT

Step 2 Operator Interview: Mr. Laurent Auriau

...

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Step 3 Installation Review and VerificationOutdoor Air Temp. Sensor

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System schedule in override. (Controls installer left test program active)

ALL

PROBLEM DESCRIPTION & EFFECT

UNIT

Step 4 Forced Response Testing and Analysis (passive w/ BEMS)

First Auto-Cx test of AHU3

- 5

0

5

10

15

20

25

30

06/10/200319:12

07/10/200300:00

07/10/200304:48

07/10/200309:36

07/10/200314:24

07/10/200319:12

08/10/200300:00

08/10/200304:48

08/10/200309:36

Temp

(°C)

-1

0

1

2

Cmd

0-1

TRA AHU3

TSA AHU3

TOA

UHC AHU3

Supply Fan

1

s t Auto-Cx testing

period without fault2n d Auto-Cx testingperiod with fault

1 am 4 a m1 a m 4 am

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First Auto-Cx test of AHU3

-5

0

5

10

15

20

25

30

06/10/200319:12

07/10/200300:00

07/10/200304:48

07/10/200309:36

07/10/200314:24

07/10/200319:12

08/10/200300:00

08/10/200304:48

08/10/200309:36

Tem

p (°

C)

-1

0

1

2

Cm

d 0-

1

TRA AHU3

TSA AHU3

TOA

UHC AHU3

Supply Fan

1s t Auto-Cx testingperiod without fault

2nd Auto-Cx testingperiod with fault

1 am 4 am1 am 4 am

Step 3 Forced Response Testing and Analysis (active w/ BEMS)

First Auto Cx tests were conducted on AHU3 over two nights

2nd night- Faulty condition BEMS logic error causes pumps to cycle off

1st night- Fault free with pumps in manual override

Finding: Cooling coil is undersized for 17°C (62.6°F).**Laboratory needs are not met- fan coil units added.

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Step 3 Forced Response Testing and Analysis (active w/ BEMS)AHU2 Cooling coil capacity step test:

Return Temp. setpoint is changed from 20°C -> 19°C (3 hours) -> 18°C (3 hours) -> 17°C (3 hours)

. Auto-Cx test of AHU2

13

15

17

19

21

23

25

1/22/200414:24

1/22/200416:48

1/22/200419:12

1/22/200421:36

1/23/20040:00

1/23/20042:24

1/23/20044:48

Tem

p (

°C)

-0.5

0

0.5

1

1.5

Cm

d 0

-1

Tra,s AHU2

Tra AHU2

Tsa AHU2

Ucc AHU2

Auto-Cx testing period without fault.

Auto-Cx testing period w ith fault.Tra,s not

Finding: Cooling coil is undersized for 17°C (62.6°F).**Laboratory needs are not met- fan coil units added.

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Redesign exhaust system for AHU 1 and update design drawings

Exhaust duct from AHU1 is connected to the exhaust of AHU 3AHU1,3

Remove test programForced continual operation of AHUs due to a test program installed in 2000

AHU1, 2 and 3

AHU3

Chiller

Boilers

AHU 3

AHU1,2

AHU1, 2 and 3

AHU3

Unit

Provide sensor shadingOutdoor air temperature

Shutdown system 12 am - 5 amNighttime shutdown not in effect

Clean condenser finsCondenser is 50% fouled

Apply summer scheduleBoilers in manual override in summer

Reduce supply air temperature setpointin summer

Supply air temperature setpoint (21°C), results in nighttime heating in summer

Correct the location of the return air temperature sensor

Return air temperature sensor is located downstream of the outdoor air supply duct

Automate damper control based on outdoor and return air temperatures Operating with heat recovery in summer

SolutionFault

To-Date Results

**Green= Manual Cx Blue= Bems Assisted Cx **Orange= comfort Yellow= energy

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AHU2

Boilers

AHU3

Boilers

AHU1

AHU2, Chiller

Unit

Ensure that the circulation pump operates independent of the boiler.

AHU3 circulation pump cycles with the boiler. The heating coils are not supplied with hot water when the boilers cycle off.

Replace faulty temp sensor

Return air temperature sensor reading does not match overlay sensor, system sensor is faulty.

Reduce the open period of the boiler isolation valves to 1mn

The open period of the boiler isolation valves (3 mn) is too long for the on/off period of the boilers (2mn)

Force at least one boiler to stop

Boilers operate even when commanded off (pumps shut down, boilers still operate)

Add a dedicated pump for cooling coil

The cooling coil of AHU1 was added after the construction of the building and is connected directly to the chiller (without a separate pump) It is not possible to suspend delivery of cooling water to this AHU

Synchronize equipment operation

AHU2 is set for 24 hour operation which does not match the operation of the chilled water pumps, stopped 12am-7am

SolutionFault

To-Date Results, cont’d

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Gas Savings EstimateCorrect the boiler control logic n Boiler plant ran 24/7 to avoid occupant discomfort. n The control logic error was corrected January 5, 2004.

¨ improved comfort for occupants¨ decreased gas consumption¨ increased protection of the boiler plant equipment.

Weekly Gas Consumption vs Mean Outdoor Temp (C)

Winter Season Estimate:700€ ?10% Gas Energy Savings

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Electrical Energy Savings Estimate

Correct scheduling errors for AHUs and pumps

344574168730.1Pump Zone 4 (CW)

2833775343272070.825Pump AHU & FCU (CW)

5877370314760.169Pump Zone 5

162151964100.047Pump Zone 4 (HW)

23 x 33072795850.067Pumps Zone 1,2,3

1371830166434940.4Pump AHU & FCU (HW)

27463660833280698888Fan AHU 3

798106398580192192.2Fan AHU 2

Costsavings

Energysavings(kWh)

Energy use after Cx (kWh)

Energy use before Cx (kWh)

Power (kW)Equipment

Annual estimate:4141€ ? 47% Electrical Energy Savings

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Conclusionsn Some adaptation required for new systemsn CITE_AHU detected 3 faults in 4 automated tests

n Scheduling errors (€)n Cooling Coil & Heating coil Undercapacityn Boilers sequencing

n Development of automated tools must be used in conjunction with good protocol for system design reviews¨ Limitations to automated testing (i.e., detecting sensor

placement errors)n Quantitative energy benefits

¨ Excludes service requests¨ Equipment life¨ Heat recovery

n Non-quantitative benefits also achieved- comfort, operator knowledge, maintenance, documentation

3 yearsPay back

15000 €Project cost

5000 €Total gain

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Future developmentn Define specific test scenarios (with user-changeable parameters)n Integrate test scenarios into CITE_AHU interfacen Automate documentation of test results

¨ Incorporate required manual test and documentation archiven Test VAV systems, Expand for other configurations

n Investigate Manufacturer interest to provide integrated package.

Questions?