surfactant flushing of lnapl contaminant - clu-in surfactant flushing of lnapl contaminant...
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Surfactant Flushing of LNAPL Contaminant
Full-Scale Source and Plume Remediation of Golden UST Site:
Treatment-Train Approach
Ben Shiau, Ph.D.Surbec-ART Environmental
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Acknowledgements� Jeff Brammer, Tommy Jones, Glenn Ulrich,
Michiya Susuki, Barry Freeman (Surbec-ART)� Drs. David Sabatini, Jeff Harwell, Robert
Knox (University of Oklahoma)� Mary O�Kelley, Joe Thacker, Dick Oppel
(Oklahoma Corporation Commission)� Dr. John Wilson (US EPA)� Dr. Candida West (University of Oklahoma,
Health Science Center)
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Outline
� Recent Surfactant Flushing Development
� Laboratory Study� Field Test� Conclusions� Future Development
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Recent Surfactant Flushing Development
� Low Surfactant Concentration� Integrated Low Surfactant/
Chemical Oxidation and/or Bioamendment for Complete Site Closure
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Low Surfactant Concentration� Why this approach? Most site owners,
especially USTs and industries, have limited resources for site clean-up efforts
� Improve economics by using low surfactant concentrations (0.1 to 1 wt% versus 3 to 8 wt% in earlier Surfactant Flushing projects)
� Low surfactant challenges: formation of microemulsion (volume reduction, significant change of IFT), greater sorption impact
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Integrated Low Surfactant/Chemical Oxidation or Bioamendment Approach
� Surfactant Flushing is not suitable for dilute plume remediation
� Polishing step: injection of low chemical oxidant (< 1 wt%) and/or bioamendment to polish remaining residual / dilute NAPL plume
� Selection of chemical oxidants and/or nutrients depend on site-specific NAPL and soil properties
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Laboratory Surfactant ScreeningSurfactant system Surfactant
conc.evaluated
wt%
NAPL (TPH)solubility in
Type IIImicroemulsion
mg/L
Equilibratedtime of stable
Type IIImicroemulsion
hr
AOT/AMA/NaCl 1 to 2 440,000 1 � 2
AOT/Calfax16L-35/NaCl*
0.2 to 1 450,000 1 � 2
LubrizolDP/AMA/NaCl
0.2 to 1 400,000 8 - 12
*selected for Golden UST site
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BTEX Degradation with Oxidants
Oxidantsystem
Oxid.conc.
mg/L
Benzenedegrad.
%
Toluene
%
Ethylbenzene
%
TotalXylene
%
H2O2/Fe+2/H2SO4
2,000 92 44 59 45
KMnO4 5,000 8 NA* NA NA
*Benzene only system; Fenton�s Reagent was used at Golden UST site
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RW IW
MEUF
AS
NAPL
PERMEATE STORAGE
DisposalRETENTATE
O/WSeparator
Surfactant Flushing Integrated Process
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Golden, OK UST SiteStarting Point
� Gasoline free phase: thickness on water table 2.7 to 3.3 ft
� Shallow zone (< 15 ft) -silt:benzene, 2,000 to 36,000 µg/L in GW; TPH, non-detect to 345 mg/L
� Deep zone - sand/gravel: benzene, 50 to 3,000 µg/L; TPH, non-detect to 30 mg/L
� Surfactant Flushing Zone: 1.5 acres (22,300 ft2)
silty clay layer
Golden UST geologic cross section
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Site Well Layout
LegendDeep Well (DW)Shallow Well (SW)Horizontal WellsMLS
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Carroll�s Grocery � Surfactant FlushRemediation Well Layout Map2/6/02
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Golden UST Site, OklahomaProject Goals� Primary: Remove all free
phase gasoline� Secondary: Significant
decrease in soil and groundwater concentrations (one to two order magnitude)
� Tertiary: Soil and groundwater concentrations to primary drinking water standard
Golden UST Site, OK
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Golden, OK UST SiteApproach / Results
� Low level (< 1 wt%) surfactant/cosurfactantmixture
� 1 PV (190,000 gallons) � 60 days flushing
� Polishing: shallow -- low level chemical oxidation; deep � bioammendments(Phase I); chemical oxidation (Phase II-ongoing)
� Soil and ground water concentrations reduced by one to three orders of magnitude
0.05.0
10.015.020.025.030.035.040.045.0
mg/Kg
MLS-1A
MLS-2A
DW-1A
DW-1B
DW-5A
DW-8A
DW-16A
Benzene Concentration in Soil
Pre-floodPost-flood
0.05.0
10.015.020.025.030.035.040.0
mg/L
MLS-1A
SW-2 SW-5 SW-12
SW-14
SW-33
SW-46
Benzene Concentration in Groundwater
Pre-floodPost-flood
Data collected on 06/27/02
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Golden, OK UST SiteResults vs Goals
� Primary: no visible or instrumental evidence of free phase gasoline in 22 wells after three-month shut-down (3 had trace levels of NAPL)
� > 6,500 gallons gasoline extracted
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Golden, OK UST SiteResults (cont.)
� Secondary: GW--70% to 99% reduction in benzene concentration
� Final Polishing (Chem Oxid-Phase II) to approach MCL (12/02-expected)
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Total NAPL Recovery
0100020003000400050006000700080009000
9/16/01 11/5/01 12/25/01 2/13/02 4/4/02 5/24/02 7/13/02
Date
Gal
lons
of L
NA
PL
Rec
over
ed
Actual recovered Linear prediction
surfactant injection began
Surfactant flush+fresh water chasing
final extraction
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Golden UST Conclusion
� Surfactant Flushing appears technically and economically favorable compared with other technologies
� Significant NAPL mass removal can be achieved by low surfactant concentration approach
� Treatment-train approach -- combination of Surfactant Flushing (source removal) with chemical oxidation and/or bioamendments(contaminant plume polishing) to expedite site closure
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Golden UST Conclusion (cont.)
Economical Comparison! Total project: $712 K! Surfactant Flushing: $569 K; volume
treated = 15,550 yd3; cost = $36 / yd3
! Total project costs (including zones area treated with chem oxid) = $14 / yd3
! Properly designed, economicalAs low as: $25 - 30 / yd3 (LNAPL)
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Current & Future Surfactant Flushing Development
� Potential UST Sites for Low Surfactant Flushing: Oklahoma (2), Arkansas (1), Missouri (1), New Jersey (1)
� Tank Pit Flushing:� Free phase removal
(gasoline & diesel pits)� Love�s Country Store
(OKC, Completed--10/02) Love�s Tank Pit
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Current & Future Surfactant Flushing Development (cont.)
� Approach: low surfactant conc. (1PV)
� Different surfactant systems for gasoline and diesel pits
� Low cost ($10K-20K)� Recycling/ reuse of
recovered water� Compact design
without interrupting the routine activity Tank Pit Effluent
10/16/02
baseline
surfactant flushing