ril dahej manufacturing divsion - ciigbc award... · 1 presentation for 11th cii national energy...
TRANSCRIPT
1
PresentationFor
11th CII National Energy Award 2010
Reliance Industries LimitedDahej Manufacturing Division, India
BySh Dipak Mehta
Sh Paresh Vasava
Sh Yusuf Husain
KarmabhumiKarmabhumi
2
FTotal Area of 609 hectares having 300 hectares Green belt
FCaptive jetty- capacity for 6000 DWT vessel
FManufacturing facilities of Ethylene, Propylene, EO,
MEG,HDPE, PVC, EVA, VCM, Caustic & Chlorine
F India's Only Salt to PVC Integrated Petrochemical Complex
FCaptive Power generation capacity 155 MW
FCaptive Steam generation capacity 540 MT/Hr
FGas based Power and Steam generation
F9 MGD of surface water from River Narmada (68 KM)
Site ProfileSite Profile
Salt
Ethylene from
BarodaComplex
Semi-RichGas from
GAIL at Gandhar& Hazira
GasCrackerPlant
REON(250KTA)
EO (10 KTA)
Raw Material
C2C3
EPRU
Cl2
EO-EG Plant
VCM Plant
PVC Plant
Chlor-AlkaliPlant
C2H4
HDPE1 PlantRELENE
(200 KTA)
MEG(188KTA)
Caustic Soda Lye
(165 KTA)
30% HCl(15 KTA)
Propylene(100 KTA)
Plants
Imported Propane
Caustic Soda Flakes
(50 KTA)
Lean Gas to GAIL
Products
HDPE2 Plant
EVA PlantEVA (14 KTA)
Integrated OperationIntegrated Operation
India's Only Salt to PVC Integrated Plant
3
Certification & BenchmarkingCertification & Benchmarking
Standards Certification Date System
ISO 9001 – 2008 16th Oct 2009 Quality Management System
ISO 14001 – 2004 16th Oct 2009 Environment Management System
OHSAS 18001 - 2007 16th Oct 2009 Occupational Health and Safety Assessment Series
Plant Year Benchmarking done by Level Remarks
GCU 2009 Solomon, USA Global Ranked 1rd Quartile amongst the 30 participating plants
CPP & utilities
2009 Internal Group sites
Ranked 5th in Internal Benchmarking of RIL Group Sites
MEG 2008 PDC Netherlands Global Ranked 9th amongst MEG industries in the world.
PVC 2007 PDC Netherlands Global Ranked 4th position based on energy consumption in world
Our MissionTo be the lowest specific Energy Consumer in the industry we operateTo Minimize impact on environmentTo Widen our energy sources
Integrating energy management Upgrading Hardware and deploying new technologiesSupporting scientific researchCarrying out Audits & training of employeeBenchmark ContinuouslyPromote Awareness
Plans to achieve by
ENERGY MANAGEMENT POLICYENERGY MANAGEMENT POLICY
4
7 of 44
2007: Five Star Rating of BSC Audit2007: Five Star Rating of BSC Audit
2002: CSE Five Leaves Award to Chlor Alkali Plant2003: ISO 9001:2000, ISO 14001:2004, OSHAS 18001:1900 Certification
2004: GAIL Award for Gas Conservation2005: 1st Prize in BEE National Energy Conservation Award
2005: Three Star Rating of BSC Audit
1996: Commercial Production Started Phase - I1999: Commercial Production Started Phase - II
2006: CII Award of Excellence in Energy Efficiency
P
P
JOURNEY OF RIL, DMD.
2006: Certificate of merit by BEE 2006: Certificate of merit by BEE
2008: CII Award of Excellence in Energy 2008: CII Award of Excellence in Energy ManagementManagement
2009: RBNQA Performance Excellence Trophy2009: RBNQA Performance Excellence Trophy2009:2009:CICIII Water Conservation AwardWater Conservation Award
P
P
P
P
P
P
P
P
P
P
P
P
P
2009: 2009: GreentechGreentech Environment ExcellenceEnvironment Excellence && Safety Safety Award Award
2009: ICC Energy Management Award2009: ICC Energy Management Award
2008: CII Award of Excellence in Water Management2008: CII Award of Excellence in Water Management
P
2009: Four Star2009: Four Star for BSC Environment Auditfor BSC Environment Audit
STRATEGIC LEVEL
ñSite Presidentñ Sr. Vice President ñ Utility Cell AVPñ Utility Managers
TACTICAL LEVEL
ñ Energy Coordinatorsñ TLS Engineersñ Operation Engineer
SUPPORTING LEVEL
ñ ProcessTechnicianñ Maint. Technician
Major FunctionMajor Function : : Set TargetsProvide directionBenchmarking &External AuditsReview Utilityconsumption trendReview status of ENCON schemes and CDM
Major Function : Identification ofschemeBrainstormingSuggestionScheme
Employee & Vendor InvolvementAwarenessProgrammes
Major Function :
Evaluation ofsuggestion scheme
Monitoring SpecificUtility Consumption
Conceive new and implement schemes
Optimize utilities Consumption
Employees Involvement in Energy ManagementEmployees Involvement in Energy Management
5
Planee Obtain Insight (Audits)ee Nominate Energy Champion ee Develop Programsee Set Targets & Measuresee Develop Action Plan
Doee Implement Projectee Monitor Progressee Lock In The Gainsee Set New Targetse Communicate
Results
Checkee Review Resultsee Verify Effectivenessee Examine Opportunitiese For Continual Improvement
Actee Correct Deficienciesee Review Originalee Energy Policiesee Review Objectives &
Targetsee Review Energy Programee Update Action Plan
PD
CA
ENERGY MANAGEMENT PLANENERGY MANAGEMENT PLAN
MONITORING REPORTING SYSTEMMONITORING REPORTING SYSTEM
Video Conference with Corporate Office Top Management. Site Energy Report to bring out salient points related to energy consumption
Plant performance & energy consumption report & reviewby VP ( Technical Services)
Plant-wise report & monitoring for fuel/utilities usage by respective plant heads along with Technical service engineer
On-line monitoring tool IP-21(ASPEN PLUS) :Monitoring of Power, Steam and fuel
6
41
9
16
16
No of projects
18
0
10
8
No of Projects
with Zero Investment
8.1730.3320.662009-10
409.51
4.63
17.55
Savings achieved
(Rs. Crore p.a.)
2.37
0.80
1.26
Payback
(Months)
80.83Total
1.842008-09
Year Investment made
(Rs. Crore)
2007-08 0.33
SAVINGS IN LAST THREE YEARSSAVINGS IN LAST THREE YEARS
Eighteen Schemes were with zero investment with savings of
24.85 crores.
CO2 emission reduction achieved through various schems
in last three years is 64511 MT.
2.412.442.45
2.65
2.502.56
2.87
22.12.22.32.42.52.62.72.82.9
3
2003-04 2004-05 2005-06 2006-07 2007-08 2008-09 2009-10
Energy Index MMkcal/MT
ENERGY INDEX OF COMPLEXENERGY INDEX OF COMPLEX
Result of Consistent Efforts of RIL-DMD team
16.03 % Reduction
as compare to 2003-04
16.03 % Reduction
as compare to 2003-04
7
SPECIFIC THERMAL ENERGYSPECIFIC THERMAL ENERGY
0.911.001.05
1.28
0.00
0.20
0.40
0.60
0.80
1.00
1.20
1.40
2006-07 2007-08 2008-09 2009-10
MMKcal/MT
28.9 % Reduction
as compare to 2006-07
28.9 % Reduction
as compare to 2006-07
Contribution of various ENCON schemes
SPECIFIC ELECTRICAL ENERGYSPECIFIC ELECTRICAL ENERGY
1435
1457
15191491
1320
1370
1420
1470
1520
1570
2006-07 2007-08 2008-09 2009-10
KWH/MT
323315
313307
290
300
310
320
330
2006-07 2007-08 2008-09 2009-10
KWH/MT
Chlor alkali plant is consuming almost 45-55 %
of total power consumption of complex.
Chlor alkali Power specific Power increases with
increase in membrane Life
Based on cost benefit analysis we have replaced
the membrane in June 2009
Chlor Alkali Plant Specific Power Consumption Rest Plants Specific Power Consumption
In last four years total 9372 MWH of
power saved through various Energy
Conservation schemes
4.95% reduction of specific Electrical
Energy as compare to 2006-07
8
PROJECT
OF
PROVISION OF GAS - GAS EXCHNAGER
BEFORE PROJECT
PLAN
9
DO
AFTER PROJECT
Observations After Commissioning of New Exchanger
0.764MT/HrSteam Savings
58.6677MT/DayTotal Steam Consumption
Parameter UoM Before After
Steam consumption MT/Cycle/Day 38.50 29.33
Number of regeneration cycle
No 2 2
CHECK
10
CONCLUSIONSCONCLUSIONS
• Resulted in Energy savings of 0.39 MMkcal/Hr
• Saved Rs 60 lakhs/Yr
• Invetment of project is Rs 24 lakhs
• Payback – 4.8 months
ACT
PROJECT
OF
REDUCTION IN ENERGY DEMAND OF VCM COLUMN
11
FEED
BTM
TOP
VCM Column
VCMEDCHeavy by-products
VCM (high purity)
EDCHeavy by-products
Tray 40
COLUMN DIAGRAMCOLUMN DIAGRAM
1. Model VCM column in Aspen Plus2. Validation based on Licensor’s process
flow diagram3. Fine tuning based on present operating
parameters4. Sensitivity study 5. Trial plan based on optimized window
PLAN
12
0
20
40
60
80
100
120
140
160
180
0 10 20 30 40 50 60 70 80
Tem
pera
ture
(Deg
C)
Stages
Actual Temperature, & Aspen Temp Vs No. of stages
AspenTemp Actual Temp
Column temperature profile: Good match for Aspen Plus model and actual dataValidation – Temperature Profiles
DO
6 0.38 1.878 4.17 0.9990 0.99806 0.39 1.897 4.22 0.9991 0.99826 0.4 1.914 4.25 0.9992 0.99846 0.41 1.931 4.29 0.9993 0.99866 0.42 1.9488 4.33 0.9995 0.9987
5.9 0.38 1.8729 4.16 0.9990 0.99805.9 0.39 1.8894 4.20 0.9991 0.99825.9 0.4 1.9062 4.24 0.9992 0.99845.9 0.41 1.9233 4.27 0.9993 0.99865.9 0.42 1.94 4.31 0.9995 0.9987
5.8 0.38 1.8644 4.14 0.9990 0.99815.8 0.39 1.881 4.18 0.9991 0.99815.8 0.4 1.8979 4.22 0.9992 0.99855.8 0.41 1.9152 4.26 0.9994 0.99865.8 0.42 1.9327 4.29 0.9995 0.9987
Sensitivity Analysis
Reflux ratioPressure at top
(kg/cm2g)Top VCM (Mass Fr)
Bottom EDC (Mass Fr)Steam (MT/hr)
Reboiler Duty (MMKcal/hr)
Plant Operating Condition
DO
13
Optimized Operating Window
Top Pressure
Reflux Ratio
Reboiler Duty Steam
Top(VCM)
Bottom(EDC)
PotentialSteam Saving
Potential Saving
kg/cm2g MMKcal/hr MT/hrMass
FractionMass
FractionMT per
yearRs Lakhs Per year
6 0.42 1.9488 4.33 0.9995 0.9987 2293.173 13.50
5.6 0.37 1.831 4.07 0.9991 0.9982
Aspen Plus model based analysis
DO
Feed flow
Reflux flow
Product flow
Steam flow
Top pressure
Reflux ratio
Energy to reboiler
m3/hr m3/hr m3/hr kg/hr kg/cm2gMMkcal/
hr
Normal Operation
53.84 10.64 25.47 5270 6.00 0.42 2.39
After simulation implementation
54.11 9.60 25.34 4901 6.00 0.38 2.22
Higher capacity operation (120% of normal)
64.50 10.50 30.56 5607 6.00 0.37 2.55
Model recommendations implemented in operations
CHECK
14
CONCLUSIONSCONCLUSIONS
• The simulation model predictions were highly accurate
• Optimized VCM column reflux ratio:– Energy savings of 0.17 MMKCal/hr– Saved Rs 13.5 Lakhs per annum – No capital investment
• Increased production rate 120% – Increased feed 10.3 tonne/hr.– Equivalent to increased VCM production of 2 tonne/hr– Total revenue increase of Rs 56.25 Crores / yr (VCM)
ACT
PROJECT
OF
Reduction in energy demand of propylene refrigerant machine
15
29/
Ethylene Tower
75 m tall125 trays
Scope:
•Ethylene tower reboiler and condenser are a major consumers of propylene refrigeration (C3R) –consume more than 60% of total refrigeration.
•Aspen Plus simulation model of the ethylene tower (with peripherals) and C3R 5- stage refrigeration circuit was developed.
PLAN
16
1. Model Ethylene Tower in Aspen Plus2. Validation based on Licensor’s process
flow diagram3. Fine tuning based on present operating
parameters4. Sensitivity study 5. Trial plan based on optimized window
PLAN
Validation of ModelValidation of ModelAspen Vs Design Temperature Profile
-40
-35
-30
-25
-20
-15
-10
-5
0
1 11 21 31 41 51 61 71 81 91 101 111 121
Stage
Tem
p, °C
Aspen temperature prof ile Design temperature prof ile
DO
17
33/
28
28.5
29
29.5
30
30.5
31
31.5
32
32.5
33
33.5
0 10 20 30 40 50 60 70 80 90 100Feed tray location
Tota
l Ene
rgy(
MM
kcal
/hr)
Feed tray sensitivity
Lowest total energy consumption observed for feed on Tray 73
DO
34/
UoMSimulation
Results
(80th Tray)
Simulation Results
(76th Tray)
Feed flow TPH 83.4 83.4
Reflux flow TPH 252 246
Product flow TPH 52 52
Energy to reboiler MMkcal/hr 8.4 7.9
Energy to side reboiler
MMkcal/hr 6.45 6.45
Energy to condenser MMkcal/hr 21.04 20.52
Ethylene Product purity
Mole % 99.96 99.96
Top pressure kg/cm2g 17.5 17.5
• Theoretical best feed location is Tray 73, but does not have a nozzle• Use existing nozzle on Tray 76
DO
18
Optimized Operating Window§ Column was originally equipped with alternate feed tray
location (Tray 76), no capital investment required
§ Simulation results show that energy requirement for the column is lower on Tray 76. A trial was planned and the feed tray location of the column was changed.
CHECK
Parameter UoM Before After
Ethylene tower reflux T/hr 259 251
C3R 1st stage suction flow T/hr 262 255
C3R 2nd stage discharge flow T/hr 88.5 84.6
Steam to the C3R turbine T/hr 80 79
CONCLUSIONSCONCLUSIONS
• Ethylene tower feed tray optimization:– Reflux flow reduced from 259 TPH to 251 TPH
– C3R turbine VHP steam reduced by1000 kg/hr
• Energy savings:– 0.5 MMKcal/hr
– Rs 72 Lakhs per annum
– No capital investment.
ACT
19
CDM AND CCX PROJECTS SUMMARYCDM AND CCX PROJECTS SUMMARY
6
9
6
Payback
month
1410
1300
436
Savings
(Rs Lakhs)
744
970
220
Investment (Rs Lakhs)
CCX42000 (VER)
Utilization of excess Hydrogen generated by CA plant in CPP boiler
03
Utilization of Excess Steam in VAR of PVC Plant
02
Utilization of Process Steam in VAR of MEG Plant
Project description
27342
(CER Issued)
Total CO2 Reduction
(MT)
CDM
01
Type of project
Sr No.
CDM and CCX INITIATIVES
• Air pollution control for flue emission (e.g. Low Sulphur Fuel, Low NOx
burner, Steam/Water injection for low NOx)
• All waste chlorine is diverted to ‘Hypo unit’ in Chlor alkali plant
• Closed loop flaring system Adequate height of Flare & Boiler Stacks to
ensure minimum GLC
• Installed system for VOC control mechanical seals in pumps which
handles hazardous material / closed loop sampling / on line PPM/LEL
Detectors
• LDAR Programmes for fugitive emission monitoring
• Efficiency improvement in existing Wind Mill facility
• Installation of Solar Panels in Townships
• Move towards Alternative source of energy (Bio Gas, Wind Energy)
• Rain water harvesting pits and collecting sumps inside the factor
ENVIRONMENTAL PROJECTSENVIRONMENTAL PROJECTS
20
With 3 wind farms (61 Windmills) having a total installed capacity of 15 MW, generated 25346 MWH from 2006 to 09
Solar photovoltaic : 9.3 MWH in 2006-09
Bio gas plant installed with capacity of 100 kg/day of canteen waste normal charging rate is 25-30 kg/day
USE OF RENEWABLE ENERGYUSE OF RENEWABLE ENERGY
Bio Gas Plant Solar Panel Wind Farm
20,000 + tree
saplings planted
In 2009-10
20,000 + tree
saplings planted
In 2009-10
ENVIRONMENTAL EXCELLENCEENVIRONMENTAL EXCELLENCE
21
Back wash water was being discharge to natural water pond which has no end use. Now it is being diverted for irrigation to Jatropha plants resulted in annual water savings of 16800 m3
Use of Cooling tower blow down as a make up for fire water
Use of Mix-slop oil as a fuel - equivalent to 9605 MT Natural Gas
Use of Gas Cracker off gas & EPRU flash gas as a fuel – equivalent to 28791 MT Natural Gas
Use of Hydrogen from Chlor Alkali plant as a fuel – equivalent to 4663 MT Natural Gas
Use of cooling tower blowdown for Horticulture resulted in annual water savings of 21900 m3
RESOURCE CONSERVATIONRESOURCE CONSERVATION
ECO POND FOR MIGRATORY BIRDSECO POND FOR MIGRATORY BIRDS
22
ECO POND FOR MIGRATORY BIRDSECO POND FOR MIGRATORY BIRDS
EMPLOYEE ASSOCIATIONEMPLOYEE ASSOCIATION
• Seminars and Conferences • In house environment management system-Green card
performance rating system(GPRS)• Encourage and facilitate dialogue and participation to release
full potential of human asset at the site in the area of environment improvement
• Cascading the environmental KPIs to individual manufacturing plant/service plant/ non plant
• Offer the freedom for new environmental initiatives and reward for performance and breakthroughs
• Allocation of funds for Environment management & utilization
Total No of
employees
No. of Training Programmes
No. of Participants Percentage of total
employees trained
SafetyEnvironment
Occupational Health
Management
OfficersWorkmen
3776 61 28 29 275 173 1394 48.78
23
IMPLEMENTATION OF IMSIMPLEMENTATION OF IMS
CertificateCertificate ObservationsObservations Action takenAction taken
ISO 9001:2008
Five customer complaints for PVC were received in 09-10. As per recommendation of CTS; actions are identified to implement during shut down activity. However PVC plant persons are not aware of these complaints & planned actions although shutdown is planned from 6th May-10
Plant HOD will segregate all customer complaint in XL sheet. It will be reviewed monthly. Corrective actions required from concern department will be followed up
ISO 14001:2004
At Ethane Propane recovery plant. About
6.5 MT of spent carbon is generated.
1. It is not identified as an environmental aspect
2. Spent carbon after removal from system & kept in open area for further cooling with water. Water is going to storm water and no dyke wall provided to stop spillage on land
1. Aspect-impact register reviewed. 2. New location for storing of spent carbon is identified which is having dyke wall.
OHSAS 18001:2007
At PVC warehouse Waste drum identified for "Cotton Waste", other scarp materials & rubber items found dumped in it.
SOP will be revised for sorting of waste and its storage in the designated area
Some of Corrective/Preventive action taken based on IMS Audit
GOALS
24
Not EnvisagedNot EnvisagedComplexVFD scoping study of complex
6
EPRU
EPRU
GCU
GCU
Yard
Plant
10
200
40
150
1.2
InvestmentRs Lacs
109
80
76
100
52
SavingsRs Lacs
LP steam common header scheme for EPRU plant to reduce PRDS load
Installation of hydraulic turbine at amine contactor
Increase in residue gas exchanger area for better heat recovery
Provision of LP ethylene from GCU to VCM to offload C2R and C3R
Provision of Isolation Valve in Yard Piping phase I side
Title
5
Sr. No.
1
2
3
4
Projects Underway 2010Projects Underway 2010--1111
12.552VCMEDC Furnace-I WHB Forced Circulation
10
-Intangible/Improves operator awareness
All plants
DCS Display of Kcal/Kg of product and Kcal/hr for all plants
11
57.6127.2CTCooling water pumps corrocoating
9
1842.0MEGReplacing E 624 which a shell and tube type exchanger with a plate type heat exchanger
8
5.942.85MEG
Replacing E 521 ( Reactor feed pre heater and ensuring one phase flow going to E560 ( aldehyde stripper condensate cooler ) to prevent leaking of its tubes.
7
InvestmentRs Lacs
SavingsRs Lacs
PlantTitleSr. No.
Projects Underway 2010Projects Underway 2010--1111
25
Further Information please contactDipak Mehta – [email protected]
Paresh Vasava – [email protected] Husain – [email protected]