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Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA Symposium Tokyo, Japan September 24-25, 2012 Presented by: Patricia J. Robinson, (n,p) Energy, Inc.

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Page 1: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors

Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors

Asian ISOE ALARA SymposiumTokyo, JapanSeptember 24-25, 2012

Asian ISOE ALARA SymposiumTokyo, JapanSeptember 24-25, 2012

Presented by:Patricia J. Robinson, (n,p) Energy, Inc.

Page 2: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Presentation Outline

How do you Reduce Source Term? Value of Reducing Radiation Source Term Brief Review Technology Origin

Los Alamos National Laboratory Polymer Filtration™ Science

Engineering the Solution for Each Type of Reactor Design PWRs BWRs CANDUs

Results Opportunity for Asian Lead Units

Page 3: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

How do you Reduce Plant Radiation Source Term?

Reduce Source Term by 1) Reducing CRUD on Fuel and 2) Reducing CRUD In Primary Circuit

Sounds Simple --- But Required New Engineered Solution and New Invention

Nuclear Fuel --Before Nuclear Fuel -After

Page 4: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Initiative Value Proposition

Radiation ProtectionCollective Radiation Exposure ReductionFull Spectrum of Impact: Reduced…

Dose Rates, Contamination Levels, Hot Particles, Number of Locked High Radiation Areas

Component Reliability and Fuel Performance ImprovementReduces Root Cause for Stage #1 Seal Reactor

Coolant Pump (RCP) leak rate Increases in CRUD Induced Power Shift (CIPS) Margin Reduced Crud on fuel, improves Fuel Reliability (CILC)Less Curies Generated and Available for Transport

(CRUD)

Page 5: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Initiative Value Proposition

Outage PerformanceCritical Path Time Reduced Incremental acceleration of every small task

interfacing with RP Controls Stakeholder/ INPO-WANO/ Regulatory Risk

INPO/WANO RankingsNRC: CIPS Margin Improved, Risk Reduction RP

Related Violations Environmental Effluents (Radwaste)

Liquid Effluents -- Less Discharge of Curies --Solid Waste-- Less Filters, Less Curie Surcharge,

Less Costly Options for DisposalStakeholder Impact

Page 6: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

New Invention

US DOE R&D Labororatory for Nuclear Technology Discover science and technology, where challenges are

solved for the Medicine, Space, National security and Nuclear Technology

$4 Billion R&D Annual Budget Los Alamos National Laboratory (LANL)

118 R&D 100 awards since 1978 Invented and Patented, Polymer Filtration Technology™

Issued Exclusive World-Wide Grant of Licensed Inventions to (n,p) Energy, Inc.

R&D 100 Award-Polymer Filtration Technology (n,p) Energy, Inc. (NPE) Licensed Technology from LANL

NPE Engineered a 2 Part Solution Part 1: Reactor Shutdown Protocol (Sequence) Part 2: PRC-01M Resin Media for Rx Coolant Clean-up

Page 7: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Blue Box: Selective Binding Capability of LANL Inventions

Outlined Box: Relevant to NPP

Los Alamos N.L. ScienceR&D 100 AWARD Winner for Polymer Filtration Technology™

What Los Alamos Can do, depending on your need

Selective Capture and Removal of Specific Elements

Page 8: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

How is PRC-01M Integrated?Existing Plant Systems Chemical and Volume Control System (CVCS), Reactor Water Clean-up (RWCU), Fuel Pool Systems, Boron Recycle Systems and CANDU PHT

PWR: PRC-1 (bead) or BWR: PRC-2 (powdered)

Existing Plant Equipment PWR: Uses CVCS Demineralizer

Vessel Both: Spent Fuel Pool BWR: Filter/Demineralizers

RWCU FPC Torus

CANDU Primary Heat

Transport

Conventional

Mixed Bed

Resin-HOH

PRC-01 PRC-01

MediaMedia

PWRDeep Bed Vessel

BWRPrecoat Filter/Demin

Page 9: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Lead PlantsNPE/PRC-01 Engineered Solution

PWRs 3 Loops Turkey Point-3,4 VC Summer

PWR 4 Loops DC Cook 1,2

BWRs Peach Bottom 2,3 Monticello

B&W: Davis Besse

CANDU: Bruce A/B

Completed > 120 Refueling Outages with NPE/PRC Engineered Solution In Service

Page 10: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

NPE Engineered Solution at USA, Mexico and CanadaPWR …120 Refuleing OutagesBWR ….7 Reactors…5 Sites…20+ Refueling Outages

= LEAD PLANTS

VC Summer

St Lucie 1,2

Turkey Point 3,4

MonticelloMonticello

Beaver Valley-1,2

DC Cook-1,2

Peach Bottom-2,3Peach Bottom-2,3

Pat-San LivesHerePat-San LivesHere

Braidwood-1,2Braidwood-1,2

Laguna Verde-1,2MexicoLaguna Verde-1,2Mexico

Davis BesseDavis Besse

9 Mile Pt-1,29 Mile Pt-1,2

Page 11: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

PWR ResultsTurkey Point-3,4VC SummerDC Cook-1,2

Davis Besse

PWR ResultsTurkey Point-3,4VC SummerDC Cook-1,2

Davis Besse

QuickTime™ and a decompressor

are needed to see this picture.

Page 12: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

FPL 1st Integration 12 years Ago#1 Turkey Point 3/2000, #2 St Lucie-1 4/2000 # 3 VC Summer

Pat-San

PRC-01

Page 13: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Turkey Point-3,4 & VC SummerSource Term Approach: Only Use of PRC-01

Turkey Point 3,4: Yes: Chemistry pH(t) = 7.1 Yes: PRC-01 Media Technology No: Zinc, No Fuel Cleaning, No Elevated pH

7.2 to 7.4 Fuel Duty: Middle Fuel Duty 13 to 18 EFPY SG, Inconel 600 TT

VC Summer Yes: Chemistry pH(t) = 7.1 Yes: PRC-01 Media Technology No: Zinc, No Fuel Cleaning, No Elevated pH

7.2 to 7.4 Fuel: High Duty, AOA Susceptible 7 EFPY SG, Inconel 690 TT

Page 14: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

FPL Turkey Pt-3R18 (1st PRC)RCS Shutdown Co-58100 hrs to Clean-Up Goal

Turkey Point U3Shutdown Co-58 U3R18 (1st PRC) and R21 (4th PRC)

1.00E-03

1.00E-02

1.00E-01

1.00E+00

1.00E+01

0 10 20 30 40 50 60 70 80 90 100

Time from Shutdown, [hr]

Co-5

8, [µ

Ci/cc

]U3R18 FULL RCS

EPRI CLEAN-UP GOAL

1 E-3 uCi/cc = 37 Bq/ cc

Last RCP O/SAfter H2O2T 1/2 = 8 hr.

Page 15: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

FPL Turkey Pt-3 R20 (3rd PRC)Shutdown Co-5870 Hours to Clean-Up Goal

Turkey Point U3Shutdown Co-58 U3R18 (1st PRC) and R21 (4th PRC)

1.00E-03

1.00E-02

1.00E-01

1.00E+00

1.00E+01

0.00 10.00 20.00 30.00 40.00 50.00 60.00 70.00 80.00 90.00 100.00

Time from Shutdown, [hr]

Co-5

8, [µ

Ci/cc

]U3R20 CORE/RHR ONLY

U3R18 FULL RCS

EPRI CLEAN-UP GOAL

YELLOW SYMBOLDENOTES LAST RCP O/S

1 E-3 uCi/cc = 37 Bq/ cc

Last RCP O/SBefore H2O2T1/2 = 4 hr.

Page 16: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

FPL Turkey Pt-3R21 (4th PRC)RCSP OOS Before Peroxide InjectionShutdown Co-58 56 Hrs to Clean-Up Goal

Turkey Point U3Shutdown Co-58 U3R18 (1st PRC) and R21 (4th PRC)

1.00E-03

1.00E-02

1.00E-01

1.00E+00

1.00E+01

0.00 10.00 20.00 30.00 40.00 50.00 60.00 70.00 80.00 90.00 100.00

Time from Shutdown, [hr]

Co-5

8, [µ

Ci/cc

]U3R21 CORE/RHR ONLY

U3R18 FULL RCS

EPRI CLEAN-UP GOAL

YELLOW SYMBOLDENOTES LAST RCP O/S

1 E-3 uCi/cc = 37 Bq/ cc

Last RCP O/SBefore H2O2T1/2 = 4 Hr

Page 17: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Turkey Pt 3,4 & VC SummerSustained, Predictable Decline in Co-58 & Co-60 Shutdown Peak

Lead 3 Loop Plants ShowTREND ANALYSIS ACTUAL & FORECAST

Declining Co-58 Peaks

2.69

1.1

0.35

1.61

0.55

0.22

5.7

2.76

1.39

0.14 Actual

0.65

0.01

0.1

1

10

1st PRC 2nd PRC 3rd PRC 4th PRC Forecast

Pea

k C

o-5

8, µ

Ci/c

c

Turkey Pt 3

Turkey Pt 4

VC Summer

LESS Co-58 CURIES = LESS DOSE

EPRI G/L Clean-Up Goal 0.05 µCi/cc

0.08 µCi/cc2.96 kBq/cc

1 uCi/cc = 37 kBq/ cc

210 kBq/cc

24 kBq/cc

Page 18: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Effective Dose Rate Trending

Effective Dose Rate = Total dose for the job (mrem)

Total time for job (hour)

Good Analysis Tool for RFO to RFO Comparison Permits comparison between refueling outages

with different scope of work in containment Valid if shielding practice is consistent Valid if methods are consistent

RWP = Radiation Work Permit 1 mrem = 100 mSv

Page 19: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

FPL Turkey Pt-3Sustained Decrease in Outage EDROverall Before/After PRC-01 = - 88.4%

Turkey Pt-3 Trend Analysis Total Outage EDR (All RWPS)

5.343

3.6612.975

1.22

0.619

0.1

1

10

U31998 R17 U32000 R18PRC

U32001 R19PRC

U32003 R20PRC

U32004 R21PRC

ED

R, [

RW

P E

xp

os

ure

, mR

/ R

WP

Ho

urs

] Total Outage RWPS -EDR Stainless Steel

Co-60 Decay Curve

-31%

-18.8%

-59%

-49.3

1 mrem = 100 mSv

Page 20: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Annual Liquid Effluent DischargesCo-58 and Co-60 Trend

Liquid Radwaste Processing System: Activated Carbon, Conventional Resins- No Ultra-filtration or Reverse Osmosis

Impact of Source Term Reduction Technology Co-58 & Co-60 Liquid Radwaste Effluents Trend

Normalized to No. RFO/ Yr

27.1

2.20.7

23.8

4.45.9

2.4 1.6

34.6 (1.2 GBq)

3.9

0

5

10

15

20

25

30

35

40

1999 1 RFO

2000 1st PRC2RFOs

2001 PRC1 RFO

2002 PRC1 RFO

2003 PRC 2 RFOs

Acti

vit

y,

[mC

i] N

orm

alize

d #

Co-58

Co-60

0,05 GBq

1 mCi = 37 MBq

Page 21: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Annual Liquid Effluent DischargesFe-55 and Ni-63

Turkey Point 3,4 Fe-55 and Ni-63 Annual Liquid Radwaste Effluent Release

1.844 1.830

5.904

6.112

3.67 5.95

46.38

0

1

2

3

4

5

6

7

1999 1 RFO

2000 1st PRC2RFOs

2001 PRC1 RFO

2002 PRC1 RFO

Fe

-55

Eff

lue

nt

Re

lea

se

,

0

5

10

15

20

25

30

35

40

45

50

Ni-

63

Eff

lue

nt

Re

lea

se

,

Fe-55Ni-63

1 mCi = 37 MBq

Page 22: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Ag-110m Decline

Turkey Point 3,4 Ag-110m Annual Liquid Radwaste Effluent ReleaseNormalized to No. RFO/ yr

5.300

0.383 0.465 0.26 (0.01 GBq)

8.020 (0.297

0

1

2

3

4

5

6

7

8

9

1999 1 RFO

2000 1st PRC2RFOs

2001 PRC1 RFO

2002 PRC1 RFO

2003 PRC 2 RFOs

Eff

liu

en

t R

ele

as

e,

Ag-110m

1 mCi = 37 MBq

Page 23: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

FPL Turkey Pt. 3,4 & VC Summer Successful Source Term Reduction Summary

INPO Ranking Collective Exposure- Turkey Pt 3,4 4th Quartile in 2000, Avg RFO 140 to 160 REM 1st Quartile in 2006, 1 Unit top Decile, 52.7 REM INPO Good Practice for Source Term at Turkey Pt 3,4 and St. Lucie

1,2 INPO Ranking - VC Summer

3rd Quartile 2000, 140 to 160 REM 1st Quartile 2006, RFO16 - 52 REM TLD

Effective Dose Rate Reduction 93.3% reduction in effective dose rate for Containment RWPS 90% reduction in EDR for all RWPs

Avoided Occupational Radiation Exposure for multiple RFOs 325 REM (3.25 Sv) estimated of avoided occupational exposure

for Turkey Pt U3, same for U4 LLW Disposal Reduction Curies and Disposal Costs

$250,000 USD avoided per RFO in primary resin curie surcharge for Low Level disposal

Faster Shutdown Sequence 26 hours earlier for last RCPs to be taken out of service (O/S)

Page 24: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Turkey Point-3,4 Summary (cont.)

- 61.5% Reduction in number of High Radiation Area

- 35% Reduction in contract HP staff, $400,000 avoided costs

every RFO. - 76%

Reduction in Hot Spots - 49 X (fold)

Reduction in annual effluent activity discharged for Co-58 and 15 fold for Co-60

- 87.7 % Reduction in Ni-63 annual effluent activity discharge, and

70% for Fe-55 1st World Record Low Dose Performance for U4 in 2005.

5.407 REM (54.07 mSv) U4 RVH 2nd World Record Low Dose Performance for U3 in

2005.

Page 25: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Page 25

BenchmarkingBraidwood -1 Improving Performance

Braidwood-1 Implemented NPE/PRC Technology- A1R15 First Implementation

- A1R16 2nd Improved Implementation

Byron-1 Implemented Ortho-MacroPorous Resin - B1R15 3rd Use of Macroporous, 2nd Otho Macroporous

- B1R16 Ortho Macroporous

- B1R17 Orth Macroporous

Ni, [gr.] % Change Ni, [gr.] % Change

A1R14 4012.000 B1R15 1936.000

A1R15 3589.000 -10.5% B1R16 3500.000 80.8%

A1R16 1467.00 -59.1% B1R17 3212.00 -8.2%

Decreased CRUD = -63% Increased CRUD = 66%

NICKEL CORE CRUD RELEASE/REMOVAL

Page 26: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Page 26

Braidwood A1R16 Source Term Success: SRMP

A1R14 to A1R16 Significant Decline In Dose Rates in SG Manway Entrance and 3 ft

SG Manway Entrance: - CL -44%, HL -53%

Tubsheet MP: - CL -59%, HL -45%

Braidwood A1R14 to A1R16 Change in Steam Generator Manway Entrance Dose RatesNPE/PRC Source Term Solution A1R15, A1R16

Hot Leg and Cold Leg by SG

-55%

-40%

-52%

-55%

-69%

-40%

-46%

-66%

-80% -70% -60% -50% -40% -30% -20% -10% 0%

A - C/L

B - C/L

C - C/L

D - C/L

A - H/L

B - H/L

C - H/L

D - H/L

% Change in Dose Rates, A1R14 to A1R16

Average Decline• Cold Leg: -50%• Hot Leg: -55%

Braidwood A1R14 to A1R16 Change in Steam Generator 3 ft from Manway Entrance Dose Rates

NPE/PRC Source Term Solution A1R15, A1R16Hot Leg and Cold Leg by SG

-68%

-59%

-50%

-22%

-62%

-57%

-42%

-80% -70% -60% -50% -40% -30% -20% -10% 0%

A - C/L

B - C/L

C - C/L

D- C/L (N.D.)

A - H/L

B - H/L

C - H/L

D - H/L

% Change in Dose Rates, A1R14 to A1R16

Average Decline• Cold Leg: -59%• Hot Leg: -45%

Page 27: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

BWR

Page 28: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Monticello R22 to R23 ResultsPRC Use R22 RFO, Cycle, R23

April 2007

-28% Decline in BRAC Points Main Circuit Piping- Standardized Locations 2003 to 2007: Declined 28.5 %

-38.5% Decline RPV Effective Dose Rate R22: EDR =1.45 mRem/RWP-hr R23: EDR = 0.89 mRem/RW-hr Change: - 38.5 %

-71.1 % Fuel Floor (Fuel Move/Inspection/CRB Replace) R22: 0.78 mRem/RWP-hr R23: 0.21 mRem/RWP-hr Change: - 71.1 %

Page 29: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Vermont Yankee R25 to R26 ResultsPRC Use R25 RFO, Cycle, R25May 2007

-28% Decline in A Recirc Suction Main Circuit Piping- Standardized Locations 2005 to 2007: Declined 28.5 %

-48.% Decline IVVI RWP Dose 16.76 REM Planned IVVI RWP Dose 8.172 REM Actual IVVI RWP Dose Declined: -48%

-43.4 % Drywell RWP Dose 21.21 REM Planned RWP Drywell Dose 12.0 REM Actual RWP Drywell Dose

Page 30: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Radiation Safety Improvement ResultsLANL/ NPE Engineered Solution for Reducing Source Term

Peach Bottom 3R 15 and 2R16 Drywell Dose Rates Reduced Permited Drywell Down Post from Locked High

Radiation Area to High Radiation Area Support Outage Performance

Platform Post Removal Dose Rate 20 to 30 times Lower Dose Rate (when Benchmarked to Limerick-1)

Platform Contamination Levels 1000 times lower smearable contamination (when Benchmarked to Limerick-1)

PBAPS 3R17: Station Low Dose Record Achieved PBAPS 2R16: Station Low Dose Record Achieved

Page 31: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

BWRs

Application on Reactor Water Clean-Up (RWCU) 100% time Refueling

Expanding to Condensate Polishers Start-up Rinse In Expanding to On-Line Portion of CPS

Page 32: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

CANDU’s: Bruce PowerBruce A/B

CANDU’s: Bruce PowerBruce A/B

Page 33: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

CANDU: BRUCE POWEROperations-Maintenance-Chemistry7 Element Solution- Media is 1 Element

Only as Effective as Weakest Link

Fuel MachineFuel Machine

Reduced StallsReduced Stalls

Releases from PHT IX

Releases from PHT IX

Permit PHT Air Ingress

Permit PHT Air Ingress

MO Decrease in pHMO Decrease in pH

Conrolled Aeration/Oxygenation

Conrolled Aeration/Oxygenation

Rapid IX Change-OutRapid IX Change-Out

Optimize PHT Clean-Up ISIsolated for PHT Fill

Optimize PHT Clean-Up ISIsolated for PHT Fill

Che

mis

try

MaintenanceOperations

Filter dP MonitoringFilter dP Monitoring

Improve Boiler ID Tube Cleaning Improve Boiler ID Tube Cleaning

Page 34: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Discovery: Bruce BU7 Activity Transport Co-60 Increase 1,000 X, Sb-124 Increase 10,000 X

U7 System PHT IX Clean up Performance for Co-60 Outage Profile

1.00E-04

1.00E-03

1.00E-02

1.00E-01

1.00E+00

1.00E+01

1.00E+02

01/23/08 02/02/08 02/12/08 02/22/08 03/03/08 03/13/08 03/23/08 04/02/08

UC

i/kg

Co-60 Inlet Sb-124 Inlet

Co-60 Outlet Sb-124 Out

Power Concentration

Bruce Power

Standard PHT

Ion Exchange Resin

Shows Almost No

Removal of

Co-60 or Sb-124

Entire Outage

Bruce Power

Standard PHT

Ion Exchange Resin

Shows Almost No

Removal of

Co-60 or Sb-124

Entire Outage

New PHT Bank I/S

Page 35: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Results: PHT System Bruce B-851 OutageFull System Operability Trial PRC-01M-Li-CN

Bruce U5 PRC Operability Field Trial During Start-up PHT Clean-Up Co-60 DF with PRC-01-Li-CN In-Service

IX 6 Loading Configuration: 3 cu ft of PRC and 4 cu ft of Strong Base Anion

1.00E-03

1.00E-02

1.00E-01

1.00E+00

1.00E+01

27-Jun-12 27-Jun-12 28-Jun-12 28-Jun-12 28-Jun-12

Date

uC

i/kg

PHT Inlet ConcentrationPHT IX 6- PRC Outlet Concentration

Full Scale Operability TestNo DP Problems

No Sluice ProblemsNo D2O or De-Deut Problems

Lithiation TimeMax. DF=585 Co-60

Full Scale Operability TestNo DP Problems

No Sluice ProblemsNo D2O or De-Deut Problems

Lithiation TimeMax. DF=585 Co-60

Inlet PHT

Page 36: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Collaboration Opportunity for Asian Reactors

Technology Full Developed and Demonstrated Successful More than 10 years of Operating Experience Lead PWRs Now Lowest Dose Plants in US

DC Cook-1,2 4 Loop PWR Design VC Summer, 3 Loop Design Davis Besse, B&W Design

BWR and CANDU Solution Developed Searching for a Lead Plant in Asia

Collaboration with US NPE Engineers and LANL Exempt Technology Use License Fees Please Express Interest to Ms. Robinson

Page 37: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Thank You Very Much for Your AttentionThank You Very Much for Your Attentionご清聴ありがとうございました

Page 38: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

Metrics and Measures

RFO Shutdown& Cycle

Chemistry

FuelDuty & CIPS

TLD Dose&

PCE’s&

LHRA/HRA

CZTGamma

Spectrum

EffectiveDose Rate

Component & “Baseline”Dose Rates

DC Cook 1,2

Benchmark

Data Options

Measurement Instruments Dose Rates Baseline- CNTMT Monitors SG- SRMP Heat HX Rx Head D.R CNTMNT GA

Forced Outages Execution of Shutdown

& Outage Plan Equipment

Performance e.g CVCS Demin & Filter

Fuel Duty CIPS Core Crud &

Shutdown Release Mass on Fuel

Field Trials Gamma Spectrum Energy Emission

Rate Pipewall Deposited

Activity Estimate

Specific RWPs EDR Rx Hd R-R SG RWP

ED TLD Buyback PCE’s # of LHRA/HRA

Co-58, Ni Peak Analysis Zn/ No Zinc Cycle Co-60 Correlation with HL Dose Rates Stranded Activity- LISV

Cycle Performance &

OutageEvents

Page 39: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

CY 2000: First of a Kind Engineered Solution Developed for US PWRs

Early 1998… Collaboration Process Engaged Florida Power and Light/ LANL/ NPE

Florida Power and Light Turkey Point 3,4 Sponsored Research & Development -First of

a Kind Engineering. $1.2 M Investment by Florida Power and Light Developed Shutdown Sequence (Protocol)

and PRC-01M Media

Page 40: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

B&W Design

QuickTime™ and a decompressor

are needed to see this picture.

Page 41: Los Alamos National Laboratory Developed Technology Proven Effective for Reducing Plant Radiation Levels in Light and Heavy Water Reactors Asian ISOE ALARA

2011: Davis Besse- RVH Planned 128 REM; Actual 40 REMRFO 16 to 17M - Two Core Rotations

Davis Besse EPRI Survey Data - Engineered Solution Implemented in RFO 15

16 RFO to 17M (12 Month)

13%

-20%-25%-22%

-42%-34%

-62%

-77%

-93%

-68%

-29%-25%

-33%

-58%

50%

-32%

-100%

-80%

-60%

-40%

-20%

0%

20%

40%

60%

RC P 1 - 1SUC TION,BEND

RC P 1 - 2SUC TION,BEND

RC P 2 - 1SUC TION,BEND

RC P 2 - 2SUC TION,BEND

RC P 1 - 1DISCHARGE

RC P 1 - 2DISCHARGE

RC P 2 - 1DISCHARGE

RC P 2 - 2DISCHARGE

HOT LEG, OTSG- 1 HOT LEG, OTSG- 2 OTSG- 1 LOWERCONTAC T

OTSG- 2 LOWERCONTAC T

OTSG- 1 UP P ERCONTAC T

OTSG- 2 UP P ERCONTAC T

DH C OOLER 1 - 1INLET

DH C OOLER 1 - 1OUTLET

DH C OOLER 1 - 2OUTLET

DH C OOLER 1 - 2INLET

Location

Perc

ent C

hang

e in

Dos

e Ra

te [%

]

RCP 1-1 SUCTION,BENDRCP 1-2 SUCTION,BENDRCP 2-1 SUCTION,BENDRCP 2-2 SUCTION,BENDRCP 1-1 DISCHARGERCP 1-2 DISCHARGERCP 2-1 DISCHARGERCP 2-2 DISCHARGEHOT LEG, OTSG-1HOT LEG, OTSG-2OTSG-1 LOWER CONTACTOTSG-2 LOWER CONTACTOTSG-1 UPPER CONTACTOTSG-2 UPPER CONTACTDH COOLER 1-1 INLETDH COOLER 1-1 OUTLETDH COOLER 1-2 OUTLETDH COOLER 1-2 INLET