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Drilling a geothermal well into a deep sedimentary geothermal reservoir conclusions from case study Gross Schoenebeck Wulf Brandt & Geothermics Group GeoForschungsZentrum Potsdam

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Page 1: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

Drilling a geothermal well into a deep sedimentary

geothermal reservoir –

conclusions from case study Gross Schoenebeck

Wulf Brandt & Geothermics Group

GeoForschungsZentrum Potsdam

Page 2: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

In situ Geothermal Laboratory

Paris

Bruxelles

London

Munich

Praha

Warszawa

Berlin

Hamburg

Kobenhavn

NEGBPT

NWGBNEB

DB

NorthSea

BalticSea

Rotliegend

Tornquist zone

Variszicanbelt

Variszican Deformation front

Caledonian Deformation front

Caledonides &older massifs

Precambriancrystallinebasement

Alps

Rhenoherc

ynian

Saxoth

uringia

n

Mold

anubian

Alp

ine

front

0 100 200 km

Gross Schoenebeck

(modified after Ziegler

1990, Bertelsen 1992,

Brecht 1999)

Page 3: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

Operations overview

open hole proppant frac

Jan/Feb 2002

production test / logging

4130-4190m (frac 1)

4080-4118m (frac 2)

production test / logging

open hole waterfrac

start Jan/Feb 2003

3874-4294m, borehole instability

production test

cont. Nov/Dec 2003

4135-4309m

production test / logging

Dec 2004

injection test

April 2006 to Jan 2007

drilling 2. well

Page 4: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

0n the way to an operating doublet

well path of second well

- designed as deviated well

- in direction of minimum horizontal stress

- to optimize performance of doublet

aim

- maximization of flow rate

- for 30 years

- avoid thermal short circuit

scheduled fracture treatments

- designed to achieve PI > 30 m³/(h*MPa)

- sufficient for geothermal power production

on economic level

Page 5: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

EGS Gross Schoenebeck

Page 6: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

Borehole Design of the Research Well

Page 7: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

Lessons learned

o drilling a large diameter borehole in sheet

silicate bearing rocks (sequenzes of

sand/sandstones and clay/mudstones)

o directional drilling through and beneath rock

salt formations with plastic behaviour

o Adaptation to encountered geological

conditions requires the variability of mud

concepts with the goal of minimized formation

damage

Page 8: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

Large top hole diameter affected ROP

Insufficient pumping capacity in the

top hole region (23“) lead to bit

balling resulting in a ROP of 4…7

m/h and an increased number of

trips.

Improper bit selection reduced ROP in

the mesozoic section (16“).

Page 9: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

disastrous cementation of 16“x13 3/8“ casing

Total fluid loss occured during the

cementation of the combined casing

16“ x 13 3/8“ despite of a slurry

density of 1450 kg/m³ (Litefil by

Schlumberger) due to plugging of the

annulus by debristemperature logs

40

50

60

70

80

90

100

0 500 1000 1500 2000 2500

depth [m]

tem

p. [°

C]

temperature while caliper

logging before casing running

temperature effects of

remained cement

setting in caverns

cement losses into

Muschelkalktemperature after cementation

probable top of

solid cement

Conclusion:

Free pipe will not

stand the thermally

induced stresses to

be expected

(buckling).

Free floating pipe is

not acceptable.

Page 10: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

Recovery of casing cementation

To prevent casing damage in the future of the production well a reverse squeeze cementation through the annulus was designed and successfully performed:

temperature logs squeeze cementation

45

50

55

60

65

70

75

80

85

700 800 900 1000 1100 1200 1300 1400 1500 1600

depth [m]

tem

pera

ture

[°C

]

-6

-4

-2

0

2

4

6

8

10

tem

pera

ture

dif

fere

nces [

K]

22.9.06 before Frac

23.9.06 after Frac

23.9.06 before Cementing

24.9.06 after Cementing

DT vor/nach Frac

DT vor/nach Zem

DT vor Frac bis nach Zem.

Obviously no

annular flow

1. Free point

estimation and

cement bond

log verified top

of cement

2. Fluid loss

during injection

occurs near to

top of cement

3. Slurry density

of squeeze

cement with

1,30 below

density of mud

to be displaced

Page 11: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

Well design concepts for deep geothermal wellsHDR Soultz

fully cemented production casing partly cemented production casing suspended protective casing free moving

suspended at well head inside of polished bore receptable

Pro´s successful cementing very likely no dislocation within the casing string low costs

prevention of circulation behind the casing

cost savings no buckling

no tensile loads at the wellhead

Con´s buckling unavoidable complete cement column must be secured annular circulation possible

very high tensional load

required for avoiding buckling

only applicable in solid rocks

with no breakouts to be

expected

any fluid flow behind the

uncemented casing must

strictly be excluded

no thermally induced forces

acting on the production string

non-suspended free floating

production casing

tightness problems possible

due to casing motion

EGS Groß Schoenebeck resp. geothermal wells in sediments

Page 12: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

Casing collapse within the rock salt

9 5/8“ liner collapsed during drilling into the

target formation after reduction of mud

density from 2000 kg/m³ to 1060 kg/m³ (Heavy

deformation between 3880…3200 m)

Ovality 8 mm

Page 13: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

Cause of collapse

Casing design – according to the rules with an overburden

pressure gradient of 2,3

Casing material – successfully inspected

Anisotropic tension due to well path geometry – unlikely

according to cross-correlation

Anisotropic tension due to rock salt inhomogenities within

the salt dome in connection with the geomechanical

impact of drilling – not verifiable

Anisotropic tension due to improper cementation of the

deviated well – not very probable due to no. and

positioning of centralizers and cementing procedure

strictly following the simulation

Page 14: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

Remedy for the collaps

The loss of one

casing dimension

forced to adjust the

borehole design –

drilling of the

Rotliegend section

with 5 7/8“ and

running and

cementing of an

combined 5“ liner

with an

uncemented

section of

preperforated

pipes on bottom.

Page 15: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

Conclusions

Cost effective drilling of geothermal wells means

Considering all costs emerging over the lifetime

of the well

Design the well as tall as possible but leave one

ace upon your sleeve

With highly corrosive fluids provide demountable

coated or lined production/injection strings

Particularly to geothermal producers and

injectors adapted repair technologies for casings

should be available

Page 16: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

Tubingless insert ESP minimizes well diameter

Is the geothermal

„industry“ strong

enough to demand

such developments?

Page 17: Drilling a geothermal well into a deep sedimentary ...engine.brgm.fr/web-offlines/conference-Drilling... · Operations overview open hole proppant frac Jan/Feb 2002 production test

Repair of cemented casings

Means and technologies of expandables are to be worked out and assessed in cooperation with experienced players:

Cladded liners (casing patch)

Downhole coating of casing

Downhole relining of casing with thin (folded) metallic liners

Reasons

•Internal corrosion due to air access during production/injection

•Closing of perforations etc. (e.g. after secondary cementing)