action plan of body 0836-049
TRANSCRIPT
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Action Plan of Body 0836-049
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Part Name: Body 0836-049 Qty Found NG: 1 Pc.
Problem: Thread Damaged, with Major
Dia being observed 9.25 MM.
Problem
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A1 Blanking on Traub
A2 Centre-Less Grinding
A4
End-Mill Drilling
Thread-Rolling
Step-Drilling
A3
Chamfer
Final inspection & PA11
Flat-Drilling
A5
A6
A7
Present Process Se
Looking at the NG Component it
concluded that such component
generated at either stage.
Re-ThreadingA8
Free-Hand DrillingA9
PlatingA10
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Understanding The
- The Thread is damaged, wherein the major OD of the component is observed as 9
MM.
- Only the last couple of threads are in shape with the rest being completely damage
Thread Damaged
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A1 Blanking on Traub
A2 Centre-Less Grinding
A4
End-Mill Drilling
Thread-Rolling
Step-Drilling
A3
Chamfer
Final inspection & PA11
Flat-Drilling
A5
A6
A7
Problemati
Re-ThreadingA8
Free-Hand DrillingA9
PlatingA10
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Thread-Rolling Operation
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Fault Analysis (Man)
S. No Potential Cause Validation
1 Unskilled Operator Checked skill status of operator & found upto thedesired level, with a clear understanding of the end
requirement.
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Fault Analysis (Method)
S. No Potential Cause Validation
1 Rolling Method Incorrect Observed that the process was correct, as per theindustry standards.
2 Coolant Flow Incorrect Coolant flow was correct, and was flowing evenly
on the surface
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Fault Analysis (Machine)
S. No Potential Cause Validation
1 Cycle Time (Spark Out)Inconsistent
Spark Out Time, timer controlled, and timer workingfine.
2 Hydraulic Pressure
Inconsistent
Pressure Controller working fine.
3 Roll Configuration Incorrect Stood correct with regards to the industry standard,
and the required Ra Value
4 Stopper Alignment
Incorrect
Correct, was covering the entire surface of the
component. Height also correct.
5 Hardness of the Roll
Incorrect
Was correct as per the required hardness
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Fault Analysis (Material)
S. No Potential Cause Validation
1 Variation in the Hardness Checked, and found it correct as per requirement.
2 Variation in the Dimensions Checked, and found it correct as per requirement.
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Re-Threading Operation
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METHODMATERIAL
UNSKILLED OPERATOR
Cause And Effect Diagram
Any Dimensional
Variation
Re-Threading
Method Incorrect
MACHINE MAN
Die- Size Incorrect
Cycle Time Inconsistent
Die-Setting Incorrect
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Fault Analysis (Man)
S. No Potential Cause Validation
1 Unskilled Operator Checked skill status of operator & found upto thedesired level, with a clear understanding of the end
requirement.
2
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Fault Analysis (Method)
S. No Potential Cause Validation
1 Re-Threading MethodIncorrect
Observed that the process was correct, as perthe industry standards. However, since the hand
pressure is erratic, too much of pressure results
in thread damage.
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Fault Analysis (Material)
S. No Potential Cause Validation
1 Variation in the Dimensions Checked, and found that the profile of the InputThread was correct, with the Gauge Qualifying.
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Fault Analysis (Machine)
S. No Potential Cause Validation
1 Cycle Time (Spark Out)Inconsistent
Spark Out Time, is correct, with the Operatorfollowing the required parameters
2 Die-Size Incorrect Correct.
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Why-Why Analysis (FOR OCCURRENCE
Thread flat (major dia. 9.25 observed 9.769.96.
Because of Thread damage .
Because part resting tilted .
Because component alignment was disturbed .
Because of uneven hand pressure .
Because rethreading is a manual process .
Why
Why
Why
Why
Why
Why
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Why-Why Analysis (FOR DETECTION)
Thread flat (major dia. Oversize )
Because of Thread damage .
Setting part mixed with ok parts .
Because of Operator lack of awareness .
Why
Why
Why
Why
Why
Why
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Analysis & Counter
- Results showed that it was at the time of Setting, that such NG Piece could get
generated.
1. Operators at re-Threading once again trained on how to handle Setting
Rejections.
2. Operators at Threading, also proactively trained on how to handle SettingRejections.
3. Operators at Inspection trained to remove such components.
Thread-Damage
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THANK YOU