vibration during take-off in the cockpit of concorde · one of the interesting, though specialised,...
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VIBRATION DURING TAKE-OFF IN THE COCKPIT OF CONCORDE
C G B (Kit) Mitchell* and Brian W Payne**
* Formerly Structures Department, Royal Aircraft Establishment, Farnborough
** Formerly Chief Dynamics Engineer, British Aircraft Corporation Ltd, Weybridge and Filton
Abstract
Before Concorde flew, there was concern that vibration in the cockpit during take-off could be severe.
This proved to be the case for the prototypes, made worse by undercarriage oleos with high friction that
stuck and moved very little during the take-off roll. RAE, in cooperation with BAC and Aerospatiale,
developed a computer programme that predicted vibration and undercarriage behaviour and allowed the
effect of design changes to be explored. The characteristics needed to reduce vibration were identified
as reduced friction and a softer air spring at take-off weight. This could be achieved while still absorbing
the energy of landing by using a 2-stage oleo, for which space was available. Once the required
characteristics had been identified, the project was passed to industry for further analysis and the
necessary design changes. The path to developing revised undercarriages was tortuous, involving
many tests, until undercarriages with 2-stage oleos were fitted in 1977 and reduced vibration by about
25 percent.
Introduction
One of the interesting, though specialised, technical challenges set by the Concorde project was
reducing the level of vibration in the cockpit during the take-off roll, caused by the unevenness of the
runway exciting bending of the long flexible fuselage. It was an issue that was not reported publicly,
but if it had not been successfully overcome, could have prevented the use of the aircraft from some
uneven runways and also reduced its structural fatigue life. As this account describes activities which
took place over 40 years ago, reliance has had to be placed on memory, as well as on the documents
still available. The authors therefore apologise in advance for any detailed errors or omissions
Before the prototypes flew, RAE was expecting that vibration in the cockpit during take-off would be a
problem (Zbrojek, 1965). The prototype North American XB-70 supersonic bomber was shaking its
crew during take-off at levels that NASA rated unacceptable (Irwin and Andrews, 1969). Calculations
in the USA of vibration during high speed taxying for several hypothetical SSTs predicted high
acceleration levels in the cockpit (peak vertical accelerations of more than +/- 2g). Calculations by
SNIASx for Concorde on runway 28 at San Francisco, an abnormally rough runway for which a profile
was available from NASA, predicted a peak cockpit acceleration of 3.1g. But this was probably
pessimistic, because when calculations of vibration during take-off for subsonic aircraft were compared
with flight test measurements, the measured accelerations were typically half to two-thirds of those
calculated.
_____________________________________________________
x Société Nationale Industrrielle Aérospatiale - Aerospatiale.
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At the same time, as the first generation of big jets started flying in Africa, it was found that on some
runways the vibration levels in the cockpits were borderline unacceptable. In extreme cases, this was
probably interfering with the ability of the crew to read instruments during the take-off roll. Some of
this information was from reports by pilots, some from data recorded on airliners that had been
instrumented as part of the Civil Aircraft Airworthiness Data Recording Programme (Owen, 1971).
Establishing acceptable levels of vibration in the cockpit
RAE had cockpit vibration measurements from a VC-10 and a Boeing 707 in airline service with
British Airways (Mitchell, 1970b), and was reasonably confident that the crew complained if the
incremental vertical acceleration in the cockpit exceeded about 0.5 - 0.6g (Figure 1). The curves for
VC-10 and Boeing 707 in Figure 1 were obtained by analysing film records of take-offs and landings
such as Figure 2, which shows a take-off from New York JFK. The magnitudes of the acceleration
peaks were measured by hand and plotted as exceedance curves (a count of the numbers of peaks
exceeding different values). On subsonic aircraft, much of this vibration was caused by structural
vibration of the fuselage at about 4 Hz.
The structure of Concorde is more flexible, so the first vibration mode for the fuselage occurred at 2.28
Hz. This means that fuselage bending is excited by undulations on the runway with a typical
wavelength of about 40 metres, which tend to be of larger amplitude than the undulations of about 20
metre wavelength that affect subsonic transports. RAE calculated a typical acceleration history for the
cockpit during take-off, and the late Geoff Rowland in Engineering Physics Department used the
former TSR-2 simulator at Weybridge to replicate this history, to determine whether this would provide
an acceptable cockpit environment for the flight crew. We could not make the ride in the simulator
quite as rough as the calculations predicted, because the simulator motion system was not powerful
enough. Indeed, we could not match the worst environments that pilots were already experiencing in
big jets in Africa.
A number of the BAC Concorde test crew tried the simulator, and commented that they did not believe
an airliner would ever behave like that, and that if it did, it would be wholly unacceptable. So when the
flight test instrumentation showed that at Fairford the prototype Concorde 002 was vibrating rather
more than we had achieved with the simulator, we were surprised not to be getting reports of crew
complaints (measured peak vertical acceleration at the pilot's seat was around 0.6 - 0.7g at 2¼ Hz, and
was a little higher than that being experienced in the XB-70). It was really only when the first accelerate-
stop tests were done that the crews seemed to become aware of any difficulties caused by the vibration
environment. However, during the route proving flight to the Far East by 002 mentioned below, the
Concorde prototype encountered runways more uneven than Fairford, Toulouse and Heathrow. During
one take-off, peak vertical accelerations of +/- 1.3g at 2¼ Hz were experienced at the pilot's seat, and
the crew were not slow to complain.
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Concorde vibration - measured and calculated
Royal Aircraft Establishment initially used a very complicated computer programme to calculate
vibration in a VC-10 during take-off at Boscombe Down, to compare with experimental measurements.
We found the programme was seriously overestimating the vibration experienced. The programme
took a long time to run, and was so complicated that it was difficult to use for parametric studies to
understand the causes of the effects observed.
RAE then developed a much simpler computer programme, which represented the flexible aircraft
supported by main and nose undercarriages during a take-off along a runway with a defined profile.
The springs provided by the tyres and the undercarriage air springs are non-linear - that is, the force is
not proportional to deflection - and were represented by equations that fitted characteristics measured
on test rigs.
Most importantly, both the static and sliding friction of the oleo (the oil/air spring unit that provides
stiffness and damping) were included, because it usually takes a bigger force to unstick a moveable
object than to keep it sliding*. On the prototype undercarriage the static friction was large, which
meant that small changes in end load on the undercarriage did not move the sliding leg, because it was
stuck by friction. A contributor to the high friction was a mechanism that shortened the main
undercarriage leg during the retraction cycle, but which trapped the sliding lower part of the leg
between the outer structural casing and the interior oleo mechanism, acting as a friction lock, Figure 3.
The values of the static and sliding friction were deduced from drop tests for the undercarriage. The
measured end load was different for compression and extension of the leg, and the difference was twice
the sliding friction. Initially the static friction was guessed as slightly larger than the sliding friction,
but once flight test results were available, it was possible to measure how much the undercarriage end
load could vary without the sliding leg moving.
The RAE studies concentrated on vertical vibration in the cockpit. The level of lateral vibration was
lower, but possibly as disturbing, because pilots are more sensitive to lateral acceleration. Symmetric
motion was easier to analyse and required less data, so it became the priority topic.
The army surveyed the profiles of a number of runways, including the Concorde flight test base at
Fairford, and we calculated the vibration levels we should expect. One of the reasons for a visit to
Heathrow by prototype 002 early in the test programme was to measure the vibration at a major airport,
though we did not have the runway surveyed. Once the prototypes started flying, to our surprise we
found that vibration levels during taxying were higher than predicted rather than lower, as had occurred
for every other aircraft where measurements and calculations were compared. Figure 4 shows the
history of the vertical acceleration in the cockpit and in the passenger cabin during take-off from
Toulouse by the French prototype 001. The peak acceleration in the cockpit is about 0.75 ‘g’, with
____________________________________________________________
* Friction is the force needed to move an object horizontally along a level surface, and is
proportionate to the weight of the object. The static friction is the force needed to start an object
moving, the sliding friction is the force needed to keep it moving once it has started. Static friction is
almost always larger than sliding friction, and this difference can cause vibration such as chalk
screeching on a blackboard, tyres screaming in a skid or a machine tool cutter juddering.
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many peaks exceeding 0.5 ‘g’. Much of the vibration in the cockpit was caused by bending of the
fuselage at 2.28 Hz (cycles per second)*.
The reason for the higher than expected accelerations was not hard to find. The friction for the main
undercarriage was so high that the undercarriage barely moved during the take-off roll, although the
end load in the undercarriage varied substantially during the take-off (Figure 5). The amount the end
load could vary without the sliding leg moving indicates the value of the sticking friction at that weight.
The very flexible aircraft was supported on high pressure tyres, with effectively no springing or damping
between the tyres and the airframe. The bending of the fuselage was being forced by the main
undercarriages, with the nose undercarriage contributing virtually nothing. When the correct level of
friction was included in the calculation, the stick-slip motion of the undercarriage matched real life, but
both the Aerospatiale and RAE calculations over-estimated vibration levels by about 25%. The
criterion used to obtain a single value for the vibration during a take-off was the incremental
acceleration (positive or negative) exceeded by the ten largest peaks. This was referred to as ‘delta n
ten’, Δn 10 , and is used in Figure 6 to show the effect of changing the oleo stiffness and friction during
take-off at San Francisco. Figure 1 shows how the value of Δn 10 compares with the peak incremental
acceleration during typical take-offs.
Improving the undercarriage
At RAE we looked at possible modifications to the main undercarriage, to improve the ride during
taxying and take-off. This involved increasing the pressure in the air spring, which reduces the
stiffness of the spring at take-off weight. This in turn required a small second stage oleo to provide the
initial deflection of the undercarriage during landing, because increasing the spring pressure increased
the breakout force needed to start the leg moving during a compression stroke. This was desirable
anyway, because with the original oleo, touch down felt harsh. Fortunately, there was space available
in the existing leg for the second stage oleo, because some of the early designs had proposed a double
spring. RAE then ran take-offs on the computer from all the runways for which we had profiles, testing
the effect of the undercarriage stiffness, friction and damping on vibration levels. Figure 6 shows the
results for take-off from runway 28 at San Francisco, one of the most uneven runways for which we
had a profile. The critical characteristic was the friction; if that could not be reduced by more than a
half, changes to stiffness and damping were not effective, because the oleo did not move much. The
modification to the undercarriage to include a two stage oleo was explored theoretically by RAE, using
computer modelling to study its performance during take-off and landing, and formed the basis for the
revised undercarriage proposed by BAC in September 1974 after tests of the production aircraft at
Singapore (see below).
As well as supporting the aircraft while taxying, the undercarriage has to absorb the energy of the
aircraft as it settles on the runway during landing. This is normally the dominant design case for an
undercarriage. The stroke of the undercarriage and the maximum allowable load during landing were
________________________________________________________________________________
* Different parts of an aircraft vibrate naturally at different frequencies. In an airliner in turbulence,
the tips of the wings can be seen to be bending at about 4 Hz. The fuselage tends to bend at a similar
frequency, so the vibration combines to be wing and fuselage bending.
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already set, so we had to juggle stiffness and damping to provide an almost constant load on the
undercarriage as it compressed to full stroke during a landing at a sink rate of 10 feet/sec.
Throughout this analysis, RAE was working in close co-operation with the dynamics groups of British
Aircraft Corporation at Filton and Weybridge, and Aerospatiale at Toulouse. By early 1970, the
calculations had shown what changes to the undercarriage were needed, and a major report had been
written (Mitchell, 1970a); later in 1970 the author moved on to other work. Having established what
was causing the problem and in principle how it could be solved, the task of detailed re-design of the
main undercarriage could be passed to the manufacturers of the airframe and the undercarriage, to carry
out the detailed design work necessary. This included further theoretical analyses by BAC Weybridge,
and taxy tests with the prototype 002 to measure the effect of reducing the stiffness of the air spring by
increasing the air pressure in the oleo, for test only.
That the BAC predictions were correct did not receive confirmation until the British Prototype 002
went on a tour of the Far East in 1972. Europe, Middle East, Far East and Australia were covered and
measurements of cockpit response confirmed that a problem existed. The manufacturers had cables
back that the pilots had had a rough take off ride in particular from Athens, Bangkok, Singapore and
Tokyo. There was an excellent recording system on board the aircraft and once these were received
back in the U.K. it was realised that there was definitely a problem for the pilot. There was no
structural airworthiness problem and nor was there any problem for the passengers. BAC’s approach
was to make predictions and adjust the mathematical model to get agreement with the measurements.
Making the case to fit improved undercarriages
It was agreed to run some tests with the French prototype 001 and this went to Athens in January 1973.
The conclusion was that there was a possible problem of pilot comfort, but Aerospatiale, as design
authority for the main undercarriage, considered the production aircraft would be so different from the
prototype that any modifications should be delayed until experience with the production aircraft had
been obtained.
In September 1974 the first British production aircraft 202 was flown to Singapore. Pilots from BAC,
Aerospatiale, BA, CAA and CEV (the French airworthiness authority) were on board. As BAC
expected (and had predicted), the accelerations in the cockpit were as high, or even higher, than those
measured on the prototype. After a whole series of test flights (including visits to Kuala Lumpur) the
conclusion was reached that this high acceleration at the flight deck could interfere with emergency
procedures. BAC had a solution (introducing a two stage oleo) which meant changing the design of the
main undercarriage. Athens had already re-laid their runway after the Concorde trials there, and a
decision on the undercarriage was delayed while attempts were made to persuade other airports to re-
surface runways that caused problems for Concorde. Singapore agreed and finished the work in May
1975, which was immediately followed by more tests with aircraft 202. Unfortunately they had only
put a thin skimming of tarmac on the surface and the big undulations, which excited the Concorde
fuselage, had been untouched. A further resurfacing was undertaken and yet more trials with Concorde
proved that this time the job was satisfactory. BA started a service from London to Singapore in
conjunction with Singapore Airways but this only ran for a couple of years.
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In parallel with the Concorde work, BAC had been running a series of measurements on British
Airways VC10 aircraft and had developed a method of extracting runway data which could be used to
calculate the accelerations on Concorde. This method was then used to estimate what would happen on
other BA routes. The major routes were across the North Atlantic. This meant Dulles, Washington,
and of course JFK, New York. The runways at Dulles were fine, but all indications were that JFK was
rough. BA in the meantime had taken a number of legal actions in order to get permission to use JFK.
If BA used JFK and if the BAC calculations were correct, there would be a necessity to modify the
undercarriage as there was no way that JFK would modify their runway.
BAC had been discussing with Aerospatiale for some time how to modify their undercarriage and a two
stage test undercarriage was produced by Messier, the original manufacturer, and fitted to Concorde
201, the first production aircraft. It was not possible to go to Athens or Singapore as these runways
were now nice and smooth. However it had been discovered that Casablanca, Gander in Newfoundland
and Caracas in Venezuela were all very rough.
The aircraft was taken to Gander and a series of tests were conducted over a week or more, including a
day visit to Caracas. The modification worked, as expected, and the aircraft flew into JFK for the first
time in October 1977 for a series of tests. These were partially to establish the special take off technique
necessary to avoid built up areas and of course to try out the new undercarriage, which worked well.
This undercarriage was then fitted to the whole fleet. The modified undercarriage reduced vibration
levels by about 25% at a weight of 175 tonnes. At Musée l'Air et l'Espace at le Bourget, a prototype
and a production Concorde are displayed side by side, and it is surprising how different the two
undercarriages are in detailed external appearance. Figure 7 shows photographs of the prototype and
production main undercarriages.
Because the RAE author had moved on to other work, he did not get feedback from aircrew on the
effect of the improved undercarriage suspension. But 40 years later, while helping organise a
conference for the Royal Aeronautical Society, he met several British Airways crew members who had
flown the aircraft with the original and modified undercarriage. They reported that the improvements
made a real difference for them. With the original undercarriage, the vibration was very bad,
particularly at Singapore, where early crew training was done. David Rowland (Fleet Manager
Concorde) remarked that fitting the modified undercarriage made things much more comfortable
during take-off.
Structural fatigue
RAE went into the study of vibration during take-off because of concern over the working environment
for the crew and implications for flight safety. As test results came back, it became clear that the
vibration was also causing oscillatory structural loads that could well increase fatigue damage. Before
the fatigue test of the airframe it was not possible to quantify this damage, but it provided another
incentive for improving the situation.
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Lessons from the study
The study was reported in detail in RAE Technical Report TR 70173 (Mitchell, 1970a) and a summary
paper in the Aeronautical Journal with no scale on the graphs of aircraft responses (Mitchell, 1971).
Both reports drew some general conclusions regarding undercarriages for supersonic transports. The
most important is that for a SST, the undercarriage should be designed as much as a suspension system
for taxying as it is designed to absorb energy during landing. This contrasts with the procedure for
most aircraft, where the requirements for energy absorption dominate, and the suspension characteristics
are rather left to come out as they will. The reason that SSTs are different is that the long flexible fuselage
is sensitive to excitation by the main undercarriage, and this seems to be inherent in the geometry
necessary for a supersonic airliner or bomber. The lower frequency of the bending mode of the
fuselage is affected by undulations of the runway that have longer wavelengths than those that affect
subsonic transports, and these usually have greater amplitudes. To achieve a vibration level during
taxying comparable with that of a subsonic airliner, a SST needs an undercarriage with a much lower
specific stiffness (stiffness/static load) than a subsonic transport.
This was an exciting study to be involved in, knowing that we were making a real contribution to the
success of the Concorde project. If the undercarriages had been left in their original condition, the
consequential vibration could have reduced the aircraft’s structural fatigue life. Perhaps more
importantly, the vibration environment in the cockpit could have prevented the use of the aircraft on
some uneven runways.
References
Kirk S. Irwin and William H. Andrews (1969) Summary of XB-70 airplane cockpit environmental
data NASA TN D-5449, National Aeronautics and Space Administration, Flight Research Center,
Edwards, California.
C G B Mitchell (1970a) A theoretical analysis of undercarriage loads and taxying vibration on a
supersonic transport aircraft with experimental comparisons and an assessment of modifications to
reduce ground loads Technical Report TR 70173, Royal Aircraft Establishment, Farnborough.
C G B Mitchell (1970b) Vertical acceleration in the cockpit of a subsonic transport aircraft during
take-off measured during airline operation Aeronautical Research Council Current Paper CP No 1120,
Ministry of Technology, HMSO, London.
C G B Mitchell (1971) Some measured and calculated effects of runway unevenness on a supersonic
transport aircraft Aeronautical Journal, Vol.75, pp339-343, May 1971, Royal Aeronautical Society,
London.
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E Marjorie Owen (1971) Civil Aircraft Airworthiness Data Recording Programme – Achievements in
recording and analysis of civil aircraft operations 1962-1969 Aeronautical Research Council Current
Paper CP No 1181, Ministry of Technology, HMSO, London.
J.K. Zbrojek (1965) The need for research on the cockpit vibrational environment of the Concorde
R.A.E. Technical Memorandum Aero 910, Royal Aircraft Establishment, Farnborough.
Acknowledgement
This paper is based on one written by C G B Mitchell for a Royal Aeronautical Society conference
Concorde: The Supersonic Achievement - 40th Anniversary Concorde Conference, 8th
April 2009,
ISBN 1 85768 267 X, conference reference 601, and extracts from the conference paper are published
with the permission of the Society. Proceedings of the Concorde Conference are available from the
Conference Department, Royal Aeronautical Society, 4 Hamilton Place, London W1J 7BQ.
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Figure 1 Comparison of cockpit vertical vibration during take-off for subsonic airliners
in service and Concorde 002 at Fairford (RAE TR 70173)
‘delta n ten’ Δn 10
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Figure 2 A typical take-off record from ARC Current Paper CP 1120 (Mitchell, 1970b)
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Figure 3 Sketch of the main undercarriage leg shock absorber (oleo) and leg shortening mechanism
(Mitchell, 1970a)
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Figure 4 Vertical acceleration in the cockpit and near the centre of the passenger cabin of 001 during take-off at Toulouse
(Mitchell, 1970a)
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Figure 5 Measured main undercarriage loads and deflections during three takeoffs at Fairford
(RAE TR 70173, Mitchell 1970a)
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Figure 6 Variation in the vertical acceleration in the cockpit during takeoff on runway 28 at San Francisco
as the oleo stiffness and friction are varied
Cockpit a
cce
lera
tion r
ela
tive to t
hat
with th
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tan
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underc
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iage
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Sliding leg
Oleo (inside
sliding leg)
Leg shortening
mechanism
Second oleo, inside leg
below original oleo
Prototype main undercarriage Production main undercarriage
Figure 7 Concorde prototype and production main undercarriages, as displayed at Musée l'Air et l'Espace, le Bourget