piano key weir: an innovative spillway upgrade at ... piano key weir: an innovative spillway upgrade...

Download Piano Key Weir: An Innovative Spillway Upgrade at ... Piano Key Weir: An Innovative Spillway Upgrade at Dartmouth Dam (Australia) Mike Phillips & Eric Lesleighter Presented by: Blake

If you can't read please download the document

Upload: phungthu

Post on 06-Feb-2018

224 views

Category:

Documents


1 download

TRANSCRIPT

  • Piano Key Weir: An Innovative Spillway Upgrade at Dartmouth Dam (Australia) Mike Phillips & Eric Lesleighter

    Presented by: Blake Tullis

    Utah State University

    2nd International Workshop on Labyrinth and Piano Key Weirs Nov 20-22, Paris

  • PKW 2013 - Presenter: Blake Tullis

    91 m

    180 m

  • PKW 2013 - Presenter: Blake Tullis

    Purpose of Project Develop upgrade options to pass PMF for

    Dartmouth Dam - PMF inflow = 20,000 m3/s

    - Ogee crest spillway capacity of 4,400 m3/s

    - Several upgrade options considered

    Increase embankment dam height by 3.4 m

    Replace linear ogee weir with Piano Key Weir (head = 11.4 m)

  • PKW 2013 - Presenter: Blake Tullis

    Piano Key Weir Option for Dartmouth Dam Piano Key Weir Preliminary Design

    - Initial design based on available technical publications (HYDROCOOP in France)

    - Max. head = 11.4 m

    - W = 91 m (existing spillway width)

    Piano Key Weir design progression - Test preliminary design in physical hydraulic model

    - Optimize configuration in CFD model

    - Test and confirm design in physical model

  • Initial Piano Key Weir Testing

  • PKW 2013 - Presenter: Blake Tullis

    Physical Model Study

    1:60 Scale Model

  • PKW 2013 - Presenter: Blake Tullis

    7 cycles 91m wide (total)

    Initial Testing of Piano Key Weir

    1 2 3 4 5 6 7

  • PKW 2013 - Presenter: Blake Tullis

    1,080 m3/s

  • PKW 2013 - Presenter: Blake Tullis

    10,200 m3/s

  • PKW 2013 - Presenter: Blake Tullis

    Flow constriction

    at discharges >6,000 m3/s

    Vortex formation

    Ineffective flow area

  • PKW 2013 - Presenter: Blake Tullis

    Streamlined support section

  • PKW 2013 - Presenter: Blake Tullis

    Nearly eliminated

    vortex formation

  • PKW 2013 - Presenter: Blake Tullis

    Streamlined entrance

    conditions

  • PKW 2013 - Presenter: Blake Tullis

    10,900 m3/s (11.4m head)

  • Optimisation in CFD Model

  • PKW 2013 - Presenter: Blake Tullis

    CFD Modeling (Optimization)

    Model Verification to Physical Model with 11.4 m head: - Physical model = 10,900 m3/s

    - CFD model = 10,950 m3/s

  • PKW 2013 - Presenter: Blake Tullis

    CFD Modeling (Optimisation)

    Shape of wall crest (1/2 round) ~ +2% at low to mid-range flows

    Approach depth (2m) ~ +2%

    round crest

    2m approach

    depth

    Flow

  • PKW 2013 - Presenter: Blake Tullis

    CFD Modeling

    Upstream edge of slab shape (sloped) ~ +1.6% increase

    Sloped entrance

    Flow

  • PKW 2013 - Presenter: Blake Tullis

    CFD Modeling

    Shape of block under downstream overhang to reduce flow constriction(45deg) ~ +2% for high flows

    Evaluated 1.0 Wi/Wo 1.4 1.2 ratio selected (other ratios reduced discharge)

    45deg exit support

    Flow

  • PKW 2013 - Presenter: Blake Tullis

    Structural Analysis

    Shear strength - Centre wall thickness

    changed from 1.2 m to 0.75 m

    - Upslope wall thickness changed from 0.6 m to 0.75 m

    - Meets all load cases

    45deg exit support

    One Cycle

    Flow

    Flow

  • PKW 2013 - Presenter: Blake Tullis

    Structural Analysis

    Sliding FOS > 4 (2.3 for zero cohesion)

    Overturning: - Piers under downslope

    Walls extended upstream by 3.5 m

    - Slab extended downstream by 2.0 m

    45deg exit support

    One Cycle

    Slab Extension Piers

    Extended upstream

    Flow

    Flow

  • Final Piano Key Weir Testing

  • PKW 2013 - Presenter: Blake Tullis

    Detailed Testing Phase

  • PKW 2013 - Presenter: Blake Tullis

    486.0

    487.0

    488.0

    489.0

    490.0

    491.0

    492.0

    493.0

    494.0

    495.0

    496.0

    497.0

    498.0

    0

    1000

    2000

    3000

    4000

    5000

    6000

    7000

    8000

    9000

    1000

    0

    1100

    0

    1200

    0

    Res

    ervo

    ir Le

    vel (

    mA

    HD

    )

    Discharge (m3/s)

    Stage 2 PKW vs Stage 3 PKW

    Stage 2

    Stage 3

    Dam Crest (El. 494.0)

    Parapet Wall Crest (El. 497.4)

    8,400 m3/s

    11,500 m3/s

    10% increase in capacity with

    modifications from CFD model

  • PKW 2013 - Presenter: Blake Tullis

    11,500 m3/s

    Negative pressure under downstream overhangs

    (>9,500 m3/s)

    Water impacting directly on the chute slab

  • PKW 2013 - Presenter: Blake Tullis

    Dual Aeration Splitters

    (Cycles #2 to #6):

    3m high; 4m long

  • PKW 2013 - Presenter: Blake Tullis 27

    Negative Pressure Aerated Flow

  • PKW 2013 - Presenter: Blake Tullis

    Dynamic Pressure Testing

    Weir centre wall - Frequencies not

    likely to induce resonance

    Spillway chute at jet impact location

    - High static and dynamic pressures

    - Increase chute slab thickness by 0.5m and anchor to rock

  • PKW 2013 - Presenter: Blake Tullis

  • PKW 2013 - Presenter: Blake Tullis 850 m3/s 4,000 m3/s

    8,400 m3/s 11,500 m3/s