paper 5-cmc implementation unchahar.pdf

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    CMC IMPLEMENTATION IN OBSOLETE

    ISKAMATIC TG CONTROL SYSTEM

    UNCHAHAR

    • Parsuram Saha, DGM(C&I)

    • Neeraj Agarwal, Sr. Supdt.(C&I)

    •  A.K.Goel, Sr. Supdt. (C&I)1

    NTPC UNCHAHAR

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    • SECURING FUEL SUPPLIES

    • SOARING FUEL PRICES

    • COAL QUALITY

    FUEL

    • TECHNOLOGICAL OBSOLESCENCE

    • PERFORMANCE DETERIORATION

    • LIFE EXTENSION

    AGING FLEET

    •  ASH DISPOSAL

    • CO2 EMMISSION

    ENVIRONMENTAL

    ISSUES

    • FINANCIAL HEALTH OF DISCOMs/SEBs

    • HIGH T&D LOSSES

    • REDUCTION IN GENERATION COST

    COMMERCIAL

    ASPECTS 

    3

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    R&M 

    • Phased process 

    • Huge FinancialImplication

    • Significantimplementation time

    • May require long unitshutdowns

    In-house Innovations 

    • Bridging the

    technological gapbetween old & newsystem

    • Safety featuresadopted for Inter-panel signalexchange

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    1992 - Takeover by NTPC.BFM by design but not commissioned

    1998-99 - BFM Implemented

    2008-09 - R&M of BOP carried out

    2010  –  CMC Implemented

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    Air

    Th. Pr.

    Load

    Fuel

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    Air

    Th. Pr.

    Load

    Fuel

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    Coordinated system response during

    rapid load variations, thus ensuring grid

    stability and maintaining critical unit

    parameters within safe limits.

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    CMC IMPLEMENTATION 

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    TG Desk(emergency)

    TG

    Control

    Panel(hardware)

    CMC 

    DDCMIS (CMC Logic)

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     Generator

    PT LT

    PC LC

    Boiler

    Fuel & Air

    Control

    Turbine Governor

    Valve

    MW

    Generated

    Unit LoadController

    Unit LoadSet Point

    Throttle PressureSet Point

    ThrottlePressure

    Throttle Pressure

    Controller

    d/dt+ Time Delay

    Turbine

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    Non-availability of Iskamatic cards due to obsolescence

    System safety involved with inter-panel signal exchange

    Spacing in TG Panel for new card & terminations

    Reliable coal flow measurement in volumetric Feeders

    Poor Boiler response

    Control Loop response time of Drum level control,

    furnace draft control, air flow control, etc 14

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    Identification of hardware changes

    Identification of inter-panel signal exchange

    Ensuring cards availability & other hardware

    Testing of the cards healthiness.

    Designing of TG Iskamatic Panel internal wiring changes.

    Designing, Implementation & validation of CMC logic in DCS.

    Identification of additional monitoring signals in DDCMIS

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    • Spare channels & blocks of the existing cards were used• Some of the cards were arranged from other power plants

    • Repaired some of the old cards.

    Current to Voltage convertor (AIU-12) - 02 no.

    Voltage to Current convertor (AUI-12) - 01 no.

    MAX / UMS selector (AVB-11) - 02 nos.

    NOT Gate (FA-15) - 01 no.

    OR Gate (VA-11) - 02 nos.

    Set Reset (VS-11) - 01 no.

    Relay - 02 nos.

    Signal isolator - 04 nos.

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    ANALOG INPUTS  DIGITAL INPUTS 

    CMC Load Set Point

    CMC Min. Load Set Point

    Throttle Pressure Actual

    Throttle Pressure Set Point

    CMC ON Status

    CMC OFF Status

    Turbine Follow Mode Selected

    Run Back In Action

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    ANALOG INPUTS  DIGITAL INPUTS 

     Actual Load

    Generator Frequency

    EHTC Load Set Point

    EHTC Load Reference

    TSE Upper Load Margin

    TSE Lower Load Margin

    CMC ON From ATRS To DCS

    IP Mode Selected

    LP Mode Selected

    Pressure Controller Active

    Pressure Controller ON

    EHTC Fault

    TSE Fault

    Turbine Tripped

    Frequency Influence ON

    LSR operated

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    COMMUNICATION FAILURE

    IS UNFORESEEN

    BUT

    CATASTROPHIC

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      Three tier protection implemented for taking

    care of Load set point signal failure between

    DCS & TG controls

    MAX

    CMC LOAD SET PT

    CMC MIN. LOAD SP

    EHTC PANEL INTERNAL

    FIXED LOAD SP

    (6.00 V =150 MW)

    EHTC LOAD CONTROLLER

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    CMC will be automatically switched OFF in case of :

     Any selected transmitter failure

    Communication failure

    Signal isolator failure

    EHTC card failure.

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     A separate on/off push button provided atturbine desk, directly hardwired to ATRS panel,

    for making CMC ON/OFF in case of

    any communication failure,

    any hardware failure.

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    CMC mode can be selected from OWS if :

     Air master is in Auto

    Fuel master is in Auto

    Drum Level is in Auto

    Boiler Master is in Auto

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    LP MODE SELECTED 

    CMC ON (OWS) 

    O

    R

    S-RS 

    CMC ON

    (DCS) 

    DCS

    A

    N

    D

    NO EHTC FAULT 

    TURBINE TRIP 

    PR CNTLR IN ACTION 

    IP MODE SELECTED 

    TFM SELECTED 

    RUN BACK IN ACTION 

    BLR MSTR ON AUTO 

    LOAD DEVN. < 2 %

    (CMC SP ~ EHTC SP)

    BFM SELECTED 

    MAN MODE SELECTED 

    NOT  CMC OFF

    (DCS) 

    BOTH HPBP OPEN > 2% 

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    LOAD CNTLR

    IN ACTION 

    CMC ON

    (DCS) 

    O

    R

    S-R

    R CMC ON(TG) 

    DCS /UCD  ATRS 

    A

    N

    D

    NO EHTC

    FAULT 

    CMC ON PB(TG DESK) 

    CMC OFF

    (DCS) 

    CMC OFF PB(TG DESK) 

    LOAD CNTLR

    NOT IN ACTION 

    EHTC FAULT 

    IP MODESELECTED

    (TG DESK) 

    TFM SELECTED

    (OWS) 

    RUN BACKIN ACTION 

    O

    O

    IP MODE

    SELECTED 

    CMC FAULT 

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    CMC LOAD SP

    (DCS) 

    CMC MIN

    LOAD SP

    (DCS)

    ISO-1 

    ISO-2 

    I / V

    CONV  M

    A

    X

    S

    E

    L 150 MW 

    UMS

    SEL 2

    1

    2

    LOAD

    REFERENCEPR 

    DCS /UCD ATRS 

    I / VCONV 

    2-10 V 

    4-20 mA 

    4-20 mA 

    2-10 V 

    6.00 V 

    CMC ON (TG) 

    A

    F

    Z

    12

    A

    SB

    12 

    TG MIN. LOAD SP 

    RL

    UMS

    SEL 2

    1

    2ACTUAL LOAD

    (0-250 MW) 

    LOAD SPRAISE/LOWER

    (TG DESK) 

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    Load Set Point Generation  – TSE Upper Load margins, TSE Lower

    Load margins, Unit capability & Load gradient governs the final CMC

    load set point to Turbine EHTC Controls.

    Load SP Tracking  – CMC and TG desk EHTC load set point tracks

    actual Load for smooth change-over when CMC is made ON/ OFF.

    Runback scheme  – If any ID, FD, PA, BFP or Mill trips, then machine

    will switch over to Turbine Follow mode and IP mode will be selected.

    Pressure & Frequency Infl. correction  –  Load set point to TG is

    slightly corrected to counter the changes in Throttle Pressure &

    frequency, thus ensuring stability. 30

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    Feeder speed pick-up relocated on sprocket of drag chain so

    that feeder speed becomes zero in case of drag chain breaks.

    CHAIN

    BREAKS

    Thus coal flow measurement, a vital parameter in CMC loop,

    was made more reliable. 34

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    ID/FD/PA fan IGV & Blade Pitch Control pneumatic actuatorswere replaced by motorised actuators

    Old pnematic actuators had poor reliabilty & sluggishresponse resulting in poor control loop response time.

    The new motorised actuators were faster & maintenancefree.

    This improved the response time

    of air flow, PA hdr. & furnace draft

    control loop.

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    The signal transducers used for TSE Lower & Upper marginssignals from TSE panel to DCS were :

    Non linear

    Poor accuracy

    Unreliable due to frequent breakdowns

    0-1 mA(TSE)

    0-100 mV(To DCS mV

    I/P card)

    +

     _

    100 ohm Resistor

    0-1 mA

    (TSE)4-20 mA

    (DCS)

    Overall accuracy : 5 % Overall accuracy : 0.5 %

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     Adaptive Proportional Gain, slow Integrationaction, Small derivative action

    Feed Forwards :

    Load SP change

    Target Steam Flow

    Throttle Pressure Set Point Change

    Frequency Influence Correction

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    Air

    Th. Pr.

    LOAD

    Fuel

    Oxygen

    -/+3% RAMP FOR 5 MIN 

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    -/+5% RAMP FOR 5 MIN

    Air

    Th. Pr.

    LOAD

    Fuel

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    -/+10% RAMP FOR 2 MIN

    Air

    Th. Pr.

    LOAD

    Fuel

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    Load/ Rate of

    Change (% of

    MCR per min)

    Throttle

    Pressure

    Deviation

    (Kg/cm2) 

    Flue gas O2Deviation

    (%) 

    Furnace

    Pressure

    Deviation

    (mmWC)

    SH Steam

    Temperature

    Deviation

    (deg.C)

    RH Steam

    Temperature

    Deviation

    (deg.C)

    Drum Level

    Deviation

    (mmWC)

    Steady State +/- 2 +/- 0.4 +/- 3 +/- 3 +/- 5 +/- 15

    +/-3% for 5 min. +/- 3 +/- 0.6 +/- 10 +/- 6 +/- 6 +/- 18

    +/-5% for 5 min. +/- 3.5 +/- 0.8 +/- 10 +/- 6 +/- 8 +/- 30

    +/-10% for 2 min. +/- 4.0 +/- 1.0 +/- 13 +/- 6 +/- 15 +/- 50

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    0

    5

    10

    15

    20

    25

    THR. PR. SH TEMP. RH TEMP. HEAT RATE

    5

    12 12

    21

    3

    6 6

    11 BFM

    CMC

       D   E   V   I   A   T

       I   O   N

    (Ksc) (Deg.C) (Deg.C) (Kcal.)

    * Data analysis for Load change of 3%/min. for 5 mins.

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    Coordinated system response resulted in :

    Safe Plant operation

    Improved system stability

    Enhanced operation flexibility

    No temperature excursions during Mill

    changeover or load variations

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    Increased unit Efficiency

    Reduced generation cost

    Minimisation of UI losses

    Better Control of critical unit parameters

    No thermal stresses on turbine due to reduced

    cyclic variations

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    In today’s  scenario of fast changing technological

    advancements the systems are grappling with problem of

    obsolescence.

    With innovative approach adopted for In-house modifications,

    we can overcome this challenge and that too without being

    dependent on OEM for modifying the existing system.

    This successful implementation of CMC has demonstrated thatwith the in-house expertise & resources, systems can be

    upgraded in sync with the modern technologies to further

    strengthen the system requirements.46

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    Innovation always beats the limitations by

    well planned team perseverance. It is a job

    that has no defined end point and there is

    always scope for further performance

    enhancement.

    The journey continues….. 47

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