operational improvements at the grant town power plant

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Operational Improvements at the Grant Town Power Plant Presented By: Steve Friend Sr. Plant Engineer Edison Mission O&M 2005 ARIPPA Technical Symposium

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Operational Improvements at the Grant Town Power Plant. Presented By: Steve Friend Sr. Plant Engineer Edison Mission O&M 2005 ARIPPA Technical Symposium. Improvements at the Grant Town Power Plant. Fuel Handling and Processing Ro-Pro Facility Silt System Ash Handling - PowerPoint PPT Presentation

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Page 1: Operational Improvements at the Grant Town Power Plant

Operational Improvementsat the

Grant Town Power Plant

Presented By:Steve Friend

Sr. Plant EngineerEdison Mission O&M

2005 ARIPPA Technical Symposium

Page 2: Operational Improvements at the Grant Town Power Plant
Page 3: Operational Improvements at the Grant Town Power Plant

Improvements at the Grant Town Power Plant

• Fuel Handling and ProcessingRo-Pro FacilitySilt System

• Ash HandlingBottom Ash Screw CoolersBottom Ash Piping

• Limestone ProcessingDFM

• BoilersGrid NozzlesTube ErosionCyclonesNOx Control

• DCSFoxboro Migration

Page 4: Operational Improvements at the Grant Town Power Plant

Fuel Processing and Handling

• Addition of the Ro-Pro facility has added flexibility to the fuel production process and additional means for final product cost

• Removal of the wet circuit equipment from the original preparation plant eliminated excessive reject and reduced costs of product – dewatering chemicals and equipment no longer used

• Silt system installation and modifications have allowed facility to maximize amount of lowest cost fuel to be added into final fuel blend – higher silt percentage = minimum fuel costs

Page 5: Operational Improvements at the Grant Town Power Plant

Ro-Pro Fuel Processing Facility

Page 6: Operational Improvements at the Grant Town Power Plant

Ro-Pro Screener

Page 7: Operational Improvements at the Grant Town Power Plant

Silt Feed System

Page 8: Operational Improvements at the Grant Town Power Plant

Bottom Ash Handling Improvements

• Screw Cooler capacity was approximately 20% lower than design with a 6” Pitch Auger – required running the screw cooler at higher RPM for adequate bed level control

• 7” Pitch Auger allowed screws to be slowed down – reduced erosion rates on the cooler components

• Addition of rifle bars has helped to control trough erosion but has increased wear rate on the auger

• Application of weld overlays, wear strips, and thicker materials has helped control auger wear

Page 9: Operational Improvements at the Grant Town Power Plant

Bottom Ash Screw Cooler Troughwith Rifle Bars

Page 10: Operational Improvements at the Grant Town Power Plant

Bottom Ash Screw CoolerInlet Section of Trough

Page 11: Operational Improvements at the Grant Town Power Plant

Bottom Ash Piping Modifications

• Initial design was sweep elbows on both the primary and redundant pressurized bottom ash conveying systems

• Sweep elbows had very low mean time between failures due to erosion – on the order of a few weeks

• Reconfiguration of the system using blinded tees for the direction transitions has reduced maintenance costs.

• Effective pipe rotation program has helped to further reduce ash conveying system maintenance costs

Page 12: Operational Improvements at the Grant Town Power Plant

Bottom Ash Blinded Tees

Page 13: Operational Improvements at the Grant Town Power Plant

Limestone Handling System

• Williams Direct Fired Mill for processing limestone for injection into the CFBs

• Velocity Cone did not have any impact on final product size

• Optimization of air flow though the mill has helped to produce more ideally sized product

• Installation of VFD on the product cyclone rotary valve has helped to minimize transport line pluggage and system processing delays

Page 14: Operational Improvements at the Grant Town Power Plant

DFM

Page 15: Operational Improvements at the Grant Town Power Plant

Boiler Modifications

• Erosion Control

– Sootblower lane shielding

– Economizer hanger tube tube monitoring/shielding/replacement

– Flame Spray

– Pad Welding

– Refractory Extensions

– Stainless Steel Overlay

Page 16: Operational Improvements at the Grant Town Power Plant

Combustor Tube Erosion

Page 17: Operational Improvements at the Grant Town Power Plant

Refractory Extensions

Page 18: Operational Improvements at the Grant Town Power Plant

Combustor Tube Weld Overlay

Page 19: Operational Improvements at the Grant Town Power Plant

Boiler Modifications

• Arrowhead Nozzles

– Provide nominal improvement in limestone utilization

– Backsifting is a BIG problem

– Internal stand pipe erosion now becoming a major concern

– Increased maintenance costs offsetting any benefit realized in reduced limestone consumption

– Considering repair/replacement options

Page 20: Operational Improvements at the Grant Town Power Plant

Arrowhead Nozzles

Page 21: Operational Improvements at the Grant Town Power Plant

New Nozzle being Considered as Arrowhead Replacement

Page 22: Operational Improvements at the Grant Town Power Plant

Boiler Modifications

• Cyclones

– Segmented Vortex Finders

– Narrowing of cyclone inlet opening

– Design of vertical bullnose on the cyclone inlet to narrow the opening about 10%

– Narrowing of the opening has increased inlet velocity to >75 ft/sec

– Both changes had major impacts on limestone consumption – improvement of about 20% in total when paired with the DFM optimizations.

Page 23: Operational Improvements at the Grant Town Power Plant

Vortex Finder Deformation

Page 24: Operational Improvements at the Grant Town Power Plant

Segmented Vortex Finder

Page 25: Operational Improvements at the Grant Town Power Plant

Bullnose Modification to Narrow Cyclone Opening

Page 26: Operational Improvements at the Grant Town Power Plant

Ammonia Unloading/Storage

Page 27: Operational Improvements at the Grant Town Power Plant

Ammonia Injection Skid

Page 28: Operational Improvements at the Grant Town Power Plant

DCS Modifications

• Foxboro Migration Package

– Poor availability of Bailey replacement parts and support

– Electrolytic capacitor failures

– No changes to I/O wiring

– Low cost alternative to wholesale DCS replacement

Page 29: Operational Improvements at the Grant Town Power Plant

I/O Rack

Page 30: Operational Improvements at the Grant Town Power Plant

DCS Processor Rack