me-specific service expirience march 2014

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1 < > MAN Diesel & Turbo ME Specific Service Experience March 2014 Compiled and presented by: Thomas S. Hansen ME Task Force Group

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  • 1 < > MAN Diesel & Turbo

    ME Specific Service Experience March 2014

    Compiled and presented by:

    Thomas S. Hansen

    ME Task Force Group

  • 2 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    ME/ME-C Service Experience Agenda:

    Controllers: MPC, MPC10

    Actuators: FIVA, ELVA

    Sensors: CLO no flow, sensor

    Inductive sensors

    Operating panels: ISIC DURA PC, EC MOP

    Installation: Installation types

    Summery of inspections and problems

    Countermeasures

    Changes in the pipeline

    Monitoring PMI Auto-tuning

  • 4 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Multi Purpose Controller (MPC)

    History:

    2003 ME engine is introduced

    2004 2008 Various design and production issues

    addressed

    2008 Burn-in test introduced

    2009 Major update of PCB design

  • 5 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Place of failed MPC

    Manufacturer A

    Customer Sorting Total

    X

    Delivery Quantity 703

    Engine/Shipyard 25

    Ship owner 19

    Return rate *) 6.3%

    Y

    Delivery Quantity 862

    Engine/Shipyard 27

    Shipowner 15

    Return rate *) 4.9%

    Z

    Delivery Quantity 266

    Engine/Shipyard 13

    Shipowner 1

    Return rate *) 5.3%

    January to September 2011

    Total production: 1831

    Total returned: 100 (produced in 2008-2011)

    Return rate: 5.5 %

    35

    20

    45 X Y Z

  • 6 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Customer 2008 Year

    Production

    2009 Year

    Production

    2010 Year

    Production

    2011 Year

    Production

    X 24.2% 12.7% 4.7% 1.6%

    Y 14.9% 4.2% 1.2%

    Z 9.1% 2.5%

    Re

    turn

    ra

    te *

    *)

    Manufacturer A

    11 (of 44)

    10 (of 42)

    7 (of 14)

    ~1.5 %

    28 of 1831

    X Y Z

  • 7 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    OK 46%

    Customer 12%

    Parts 88%

    FAIL 54%

    Part No. Part Name PCB Quantity Part No. Part Name PCB Quantity

    49 74HCT245 0340 1 1450 54V, 400W 0350 3

    63 IDT7007S55JI 0350 2 1485 33V 1.5kW 0370 1

    612 3V9 0370 3 1495 MRF4 0350 1

    617 2AT 0370 1 1522 TL7705 0350 3

    620 24MHz 0350 1 1601 20IMX4-1515-8 0350,0360 2

    628 1u 100V 0370 2 1622 36V . 400W 0350 2

    629 33V 5KW 0370 5 1662 12A 0370 2

    1167 HCPL0600 0350 3 3004 10u, 35V 0350 1

    1193 HLMP-4000 0350 2 3215 XC95144 0340 1

    1370 40R2 0.1% 0350 1 4291 RELAY, 12V 0370 1

    Analysis of MPCs

    returned in 2011

    The failure parts were random and various

    Manufacturer A

    100

    46 54

    6 (see next slide...)

    48 (see examples in

    below table...)

    .

  • 8 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    China

    shipyard

    (Broken)

    Engine shop

    (Crack)

    Shipowner

    (Burnt: ESD)

    Shipyard

    (Oil)

    Engine shop

    (Damage)

    Shipowner

    (Wire: foreign

    substance) Photos of scrapped products returned from the customers

    Manufacturer A

  • 9 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    1. Production of MPCs during the period: 500

    2. Number of returned MPCs during the period: 5 (1 pending)

    3. Return rate: 1.0 %

    4. Failure rate:

    - of returned MPCs produced in 2009 and 2010: 0.8 %

    - of returned MPCs produced in 2011: 0.0 %

    Manufacturer B

  • 10 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    MPC10 Dedicated CCU

  • 12 < > MAN Diesel & Turbo THH/dept LDT ME service experience March 2014

    MPC10 Service experience

    January 2012:

    Introduced for new orders.

    Number produced:

    ~ 3000

    Reported claims

    Part damaged during production corrective action taken

    Foreign particle entered during engine production

    BGA burnt due to component failure

  • 13 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    ME/ME-C Service Experience Agenda:

    Controllers: MPC, MPC10

    Actuators: FIVA, ELVA

    Sensors: CLO no flow, sensor

    Inductive sensors

    Operating panels: ISIC DURA PC, EC MOP

    Installation: Installation types

    Summery of inspections and problems

    Countermeasures

    Changes in the pipeline

    Monitoring PMI Auto-tuning

  • 15 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    FIVA with Linear Motor

  • 16 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Linear Motor with Moving Magnet

  • 20 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Old Bearing after approx. 10.000 Hrs.

    Bearing very worn

    Bearing very worn

  • 21 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    New Bearings in Production

  • 22 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Running-in filter, FIVA & Hydr. Pumps Shop test and sea trial

    Many FIVA pilot valves are damaged during shop- and sea trial.

    Damage is causes by particles released from the piping system.

    In service, ME filter and purifiers gradually makes the oil cleaner.

    To prevent this damage, we recommend using of temporary 5 m filter between the pilot valve and the main body of the FIVA valve, during

    shop test and sea trial.

    The same filter type is also used before the pilot valves on the mechanically driven hydraulic pumps.

    The filters are removed after sea trial

  • 23 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Running-in filter, FIVA & Hydr. Pumps Shop test and sea trial

  • 24 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Running-in filter on FIVA Valves Shop test and sea trial

    Subplate

    5-micron filter cartridge

    Pilot valve

    Main valve

    Running-in filter

  • 25 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Running-in filter on Hydraulic pump Shop test and sea trial

  • 26 < > MAN Diesel & Turbo THH/dept LDT ME service experience March 2014

    ELVA Problem and countermeasure

    Challenge:

    Many failures of the original CWAT ELVA

    Always related to the ON/OFF control valve

    Action:

    Solution with an MOOG ON/OFF control valve installed with reuse of the main valve body has been service tested with a successful result

    Decision has been made that all existing vessels with ELVA are being modified to Moog-ELVA

  • 27 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    ELVA Photos

    Original version New version

  • 28 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    ME/ME-C Service Experience Agenda:

    Controllers: MPC, MPC10

    Actuators: FIVA, ELVA

    Sensors: CLO no flow, sensor

    Inductive sensors

    Operating panels: ISIC DURA PC, EC MOP

    Installation: Installation types

    Summery of inspections and problems

    Countermeasures

    Changes in the pipeline

    Monitoring PMI Auto-tuning

  • 30 < > MAN Diesel & Turbo THH/dept LDT ME service experience March 2014

    CLO Level Switch History

    History:

    2003 The sensor is introduced on ME engines PLCA-50

    2003-7 Many false alarms

    2008 The design was modified and the claim rate much reduced

    2010 Many claims of low insulation due to varistor type/

    quality (RBedia# < 2 M & Rcomp < 70.0 K)

    2010 Design was changed to achieve much improved

    insulation properties

    2011 Only improved type

    (CLS-50) is delivered

    Soldering point

    Hole in wire

  • 31 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    History of Pepperl & Fuchs Sensor for

    Exhaust Valve

    History:

    2008 Many failures reported

    2009 W42 Thorough production improvements

    2010 Jan. Stock is returned to manufacturer for checking

    2010 Temporary introduction of 2 out of 100 HASA testing (destructive testing) of delivered

    sensors

    2010 2012 No sensors of improved version has failed due

    to design or quality

  • 35 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    ME/ME-C Service Experience Agenda:

    Controllers: MPC, MPC10

    Actuators: FIVA, ELVA

    Sensors: CLO no flow, sensor

    Inductive sensors

    Operating panels: ISIC DURA PC, EC MOP

    Installation: Installation types

    Summery of inspections and problems

    Countermeasures

    Changes in the pipeline

    Monitoring PMI Auto-tuning

  • 37 < > MAN Diesel & Turbo THH/dept LDT ME service experience March 2014

    ISIC DURA PC Restart MOP Problem History

    March 2012: Reports of DURA

    PC MOP reporting restart MOP

    event log purge

    March 2012: Investigation in

    LDT/LDE department is

    launched

    April 2012: Investigation result

    and proposed countermeasure

    is agreed with maker (ISIC)

    June 2012: Hardware kit is

    finalized

    August 2012: Software upgrade

    is ready

  • 38 < > MAN Diesel & Turbo THH/dept LDT ME service experience March 2014

    ISIC DURA PC Restart MOP Problem Problem description

    Problem description

    During scheduled clean-up of event log data base, a read/write error can

    cause the MOP to stop and request restart.

    Identified related software issues

    Event log database algorithm is intolerant towards any read/write failure.

    Identified related hardware issues

    1/ Weak connection between harddisk cradle interface pcb and harddisk

    2/ Harddisk cradle resonance

    Problem is a combination of hardware and software problem

  • 39 < > MAN Diesel & Turbo THH/dept LDT ME service experience March 2014

    Hard disk cradle and interface PCD replaced with direct connection

    ISIC DURA PC Restart MOP Problem Countermeasures

  • 40 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    EC-MOP Designed by MAN Diesel & Turbo

    Advantages:

    More robust and reliable

    Lower cost

    Very low heat dissipation

    Only the necessary interfaces

    MDT owned design

    Simple installation/cabling

    MDT look and feel

    Only one new type of MOP

    Only one new software image

  • 41 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    EC MOP

    Number delivered: ~900

    Number claims: 25

  • 42 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    EC MOP

    Investigations:

    USB port failure:

    USB board U4, the IC showed was burned

    and cracked. The root cause is believed to

    be an Iinternal electrical breakdown in the

    touch controller board causing the USB

    board to breakdown

    Touch screen calibration:

    Some cases of incorrect touch screen

    calibration where found. The problems were

    found to be related to the production

    procedues which was corrected.

  • 43 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    ME/ME-C Service Experience Agenda:

    Controllers: MPC, MPC10

    Actuators: FIVA, ELVA

    Sensors: Position sensor for hydraulic pump

    CLO no flow, sensor

    Inductive sensors

    Operating panels: ISIC DURA PC, EC MOP

    Installation: Installation types

    Summery of inspections and problems

    Countermeasures

    Changes in the pipeline

    Monitoring PMI Auto-tuning

  • 45 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Agenda

    1 ME-ECS installation types historically and present standard

    2 Summary of inspection reports

    3 Countermeasures

    4 Changes in the pipeline

  • 46 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    ME-ECS: ME Engine Control System Installation types

    Engine ECR

    Classic ME-ECS control panel

  • 47 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    ME-ECS: ME Engine Control System Installation types

    Engine ECR

    ME-ECS control panel for China

  • 48 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    ME-ECS: ME Engine Control System Installation types

    Engine ECR

    Engine-mounted Control Cabinets (ECC) new standard

  • 49 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    ME-ECS: ME Engine Control System Installation types

    Engine ECR

    Common Control Cabinets (CCC) - option

  • 50 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Summary of Inspection Reports Engine builder installations

    Junction box wiring causing isolation errors:

    Wires touch the interior faces of the box and rub against them due to vibrations

    Wires get wedged between box and lid

    Cause: Wires have not been cut to length and are

    insufficiently strapped!

  • 53 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Summary of Inspection Reports Yard installations

    EICU installations in ECR

    Excessive wire length

    Units installed without cabinet

    Insufficient strapping and marking of cables & wires

  • 54 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Summary of inspection reports Yard installations

    Cable routing, marking and screen termination

    Insufficient cable marking

    Missing or wrong cable glands

    Wrong screen termination in cable glands

    Resulting in:

    More complicated troubleshooting

    Great risk of insulation faults or short circuits

    EMC problems

  • 56 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Countermeasures Updated Production Specification

    Our Production Specification for Mounting and installation of electrical

    equipment has been updated, focusing on:

    New installation types (ECC w. MPC10)

    New screen terminations in selected locations

    Junction box wiring

  • 57 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Countermeasures Implemented design changes

    Introduction of ECC, Engine-mounted Control

    Cabinets:

    Elimination of PDB and safety system box on the control panel

    EMC cable glands replaced by screen termination on controllers & grounding bars

  • 58 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Countermeasures Design changes implemented

    EICU cabinet introduced:

    One cabinet for both EICU A & B

    No cable glands: all cables enter through the bottom of the

    cabinet with screen termination on a steel comb

    Cables are connected to a terminal row with spring-loaded

    push-in terminals, leaving the electronics untouched

  • 59 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Countermeasures Junction box requirements

    To counteract the many insulation faults in junction boxes, a set of requirements

    have been defined specifically for the junction box design and wiring.

    Important highlights are:

    Wires must be cut to correct length excessive wire length is not acceptable

    Wires must be tied securely, preferreably to support bars

    Wires must under no circumstances touch the interior parts of the box or the box itself

  • 60 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    ME/ME-C Service Experience Agenda:

    Controllers: MPC, MPC10

    Actuators: FIVA, ELVA

    Sensors: Position sensor for hydraulic pump

    CLO no flow, sensor

    Inductive sensors

    Operating panels: ISIC DURA PC, EC MOP

    Installation: Installation types

    Summery of inspections and problems

    Countermeasures

    Changes in the pipeline

    Monitoring PMI Auto-tuning

  • 62 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    PMI Auto-Tuning. Standard on engines

    contracted after April 1st 2013

  • 63 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Auto-Tuning

    Potential Fuel Reduction

    Pure pmax level increase

    Potential 5-10 bar

    Potential 1-2.5 g/kWh

    Reduction in fuel oil consumption / CO2 emissions

    1 bar increase in average pmax => 0.20-0.25 g/kWh decrease in fuel oil consumption

    Reference pmax

    Potential

    Potential

    Balancing + pmax level increase

    Potential additional 2-5 bar

    Total potential 1.4 3.75 g/kWh

    Will also benefit engines already being

    operated within recommended limits

  • 64 < > MAN Diesel & Turbo ME service experience March 2014 THH/dept LDT

    Continuous auto-tuning activated

    Reference pmax

    Average pmax

    Result: 4-bar pmax increase

    1-1.2 g/kWh SFOC reduction

    PMI Auto-Tuning

    10K98ME-C

  • 65 < > MAN Diesel & Turbo THH/dept LDT ME service experience March 2014

    MOP screen for PMI auto-tuning

    PMI Auto-Tuning. Standard on engines

    contracted after April 1st 2013

  • 66 < > MAN Diesel & Turbo

    All data provided in this document is non-binding.

    This data serves informational purposes only and is especially

    not guaranteed in any way. Depending on the subsequent

    specific individual projects, the relevant data may be subject

    to changes and will be assessed and determined individually

    for each project. This will depend on the particular

    characteristics of each individual project, especially specific

    site and operational conditions.

  • 67 < > MAN Diesel & Turbo

    Thank you for your attention

    Questions?