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DRY SOLIDS PUMP COAL FEED TECHNOLOGIES DOE/NETL Cooperative Agreement DE-FE0012062 > Timothy Saunders, Program Manager > DOE Gasification and C&CBTL Workshop Morgantown, WV August 10, 2015

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DRY SOLIDS PUMPCOAL FEED TECHNOLOGIES

DOE/NETL Cooperative Agreement DE-FE0012062

> Timothy Saunders, Program Manager

> DOE Gasification and C&CBTL Workshop

Morgantown, WV

August 10, 2015

DOE C & CBTL Workshop 2DOE C & CBTL Workshop 2

Program Background

US Department of Energy (DOE) funded AR to develop:

- “A commercial solids pump as soon as possible”

Recognizing:

• Need for gasifier commercial solids pump capable of 500-1,000 PSI injection

– To reduce capital cost of Integrated Gasification Combined Cycle, Coal-to-Chemical and Coal-to-Liquid gasification based plants

• GTC analysis shows significant gasification growth to 2030 and beyond

– Electric utilities in EPRI “Coal Fleet” voted solids feeding as # 1 priority for successful commercialization of gasification plants

– Opportunity represents several 100’s solids pumps

Target date for availability of commercial pumps around 2017

DOE C & CBTL Workshop 3DOE C & CBTL Workshop 3

Program Objectives

Overall:

• Develop a solids pump that meets AR “Compact Gasifier” requirements

- 1200 psi, 400 TPD (demonstration)

• Develop a solids pump meeting commercial gasification industry requirements

- 500 psi, 600 TPD

Current Program :

•Design, develop, manufacture and test a prototype solids pump capable of

“Commercial scale” feed rate

• Test prototype to allow design optimization for commercial solids pump

Future:

• Manufacture and supply a solids pump for commercial validation

• Commence production of solids pumps for commercial sale

DOE C & CBTL Workshop 4DOE C & CBTL Workshop 4

Program Technical Approach

• Design prototype at “commercially defined” size

- 400 TPD Nominal, 600 TPD Maximum

• Utilize commercial components to maximum extent possible

• Utilize a manufacturing integrator for ensuring machine produceability

• Evaluate and test with commercially selected and supplied feed-stocks:

- Initially Illinois #6 and Powder River Basin coals,

- Then lignite, Pet Coke and coal/biomass blends

DOE C & CBTL Workshop 5DOE C & CBTL Workshop 5

Coal Feed Testing Program

To validate commercial-scale feeding system for gasifier demonstration plant

Feed Distribution System (Completed)

• Capability tested at 600 TPD (2010)

Solids pump (Underway)

- Discharge 400+ TPD at 1,200 psi

- Standard “Utility” grind PSD

- Testing multiple feed-stocks

Ultra-dense flow transport

(no plugging)

Flow splitters

(uniform distribution)

Pump

(accurate injection)

DOE C & CBTL Workshop 6DOE C & CBTL Workshop 6

Pump Operation

Normal

Loads

Normal

Loads

Tractive

Force

Track

DirectionTrack

Drive

Sprocket

Drive

Rotation

Solids Plug Load

(Gas + Friction)

System

Pressure• “Caterpillar” track moving walls

forming parallel sided duct

• Operation based on “solids lock-up” physics which achieved coal injection into 1,000 PSI in prior DOE-funded tests

• Design uses “solids plug” gas seal

also proven in prior DOE-funded

research

• “Linear” concept offers advantages over rotary solids pump:

– Higher energy efficiency

– Simply scalable to large capacities

– Feed material flexibility

Internal

“Bridges”

Carrying

Load to

Walls

Solids Flow

Direction of

solids

consolidation

DOE C & CBTL Workshop 7DOE C & CBTL Workshop 7

Prototype Pump Configuration

Inlet Isolation ValvePump Weight:

50 MT

Microwave sensors

Hydraulic Motors

Fines Bins

Outlet Pressure Vessel

Outlet Isolation Valve

Mounting

Hopper Flange

Gasifier System Flange

Pump Power

750 Kw

(2 x 375Kw)

Pump Height

5.3 m

DOE C & CBTL Workshop 8

Pump Internal Components

DOE C & CBTL Workshop 9

Pump Manufacture & Installation

DOE C & CBTL Workshop 10

Pump Installed in EERC Test Stand

DOE C & CBTL Workshop 11

Prototype Testing

• Shake-down testing initiated 2012

- Validated controls system and mechanical operation and characterization

- Confirmed fundamental operating criteria

- Identified performance limitations on certain components

• Modified select internal components for improved performance 2013

- Fines sealing around moving components

- Component clearance reductions for gas seal improvement

- Fines clearing and removal system upgrades

• Pump start-up and operation procedures developed

• DOE contract concluded end 2013

DOE C & CBTL Workshop 12

Coal Feed Technologies, CFT Program

Follow-on CFT program agreed with DOE with completion late 2016

Target 500 hours of prototype operation addressing:

- Short-term testing at pressures up to 300 PSI

- Performance mapping tests to understand and control upset conditions

- Additional feedstock tests to validate pump operation with wider range of fuels

- Long duration testing at pressures up to 1200 PSI

- Define prototype component modifications for commercial pump design

DOE C & CBTL Workshop 13

CFT Program Prototype Testing

Testing undertaken to confirm:

- Pump loading and seal plug formation

- Seal plug permeability/leakage

- Feeding at 50 t/hour into 100 psi

-450

-400

-350

-300

-250

-200

-150

-100

-50

0

50

0

5,000

10,000

15,000

20,000

25,000

30,000

35,000

40,000

45,000

50,000

0 1 2 3 4 5 6 7 8 9 10

Scra

pe

r St

rain

(u

in/i

n)

Torq

ue

(ft

-lb

f)

Tile #

Ill#6 - Plug Generation1 scfm Sparge Gas, 3.5 RPM/min -Target 40,000 ft-lbf

Ave Torque

Center Strain

Corner Strain

-800

-700

-600

-500

-400

-300

-200

-100

0

100

200

300

0

10,000

20,000

30,000

40,000

50,000

60,000

70,000

0 200 400 600 800 1000 1200 1400 1600 1800

Scra

pe

r St

rain

(uin

/in

)

Torq

ue

(ft-

lbf)

Time (seconds)

CTB-2b - 15 PSIG Ill#6 - 1 scfm Sparge Gas1 RPM/0.092 ft/sec - 40 Hz Blower Motor

Ave Torque

East Corner Strain

East Center Strain

Scraper Temp

-1000

-800

-600

-400

-200

0

200

400

0

10,000

20,000

30,000

40,000

50,000

60,000

70,000

80,000

90,000

100,000

0 200 400 600 800 1000 1200 1400 1600

Scra

pe

r St

rain

(uin

/in

)

Torq

ue

(ft-

lbf)

Time (seconds)

HPTA-1-15-55-2 - Cut on Torque - 45 seconds short of Hopper Duration1 RPM/0.092 ft/sec - 40 Hz Blower Motor

Ave Torque

East Corner Strain

East Center Strain

Scraper Temp

DOE C & CBTL Workshop 14

CFT Prototype Operational Issues

Tile-to-Tile Leak paths

Coal accumulation on drive sprockets affects

track trajectory

-1300

-800

-300

200

700

1200

-30,000

-10,000

10,000

30,000

50,000

70,000

90,000

0 10 20 30 40 50 60 70 80 90 100

Scra

pe

r St

rain

(uin

/in

), T

en

sio

ne

r P

res

(psi

g)

Torq

ue

(ft-

lbf)

Tile #

ETS-2 - 15 PSIG Ill#6 - 1 scfm Sparge Gas1 RPM/0.092 ft/sec - 30 Hz Blower Motor

Ave Torque

East Corner Strain

East Center Strain

West Tensioner Pres

Coal consolidation impacted by flow discontinuity

DOE C & CBTL Workshop 15

CFT Program Initial Results

Pump fundamentals demonstrated in CFT Prototype testing at EERC:

- Plug consolidation to density of 60 lb/ft3 repeatable

- Motor torque required – 80,000 ft-lbf

- Static plug sealed 300 psig for planned 30 minutes

- Dynamic extrusion against 55 psig for 27 minutes at 51 TPD

Coal plug delivered against gas pressure of 97 psig

Issues limiting prototype performance:

- Coal transition irregularities from dynamic to stationary zones disrupting seal

- Leakage between tiles and casing impacting track trajectory

- Plug generation beyond optimum location in flow path causing high torque

Prototype feed pressure capability and feed rate shown limited

The most effective solution to these challenges sought

DOE C & CBTL Workshop 16

Semi-scale Program

Prototype pump size, weight - has been a challenge for development:

- One year to design, build, install and test initial component modifications

- Development at full scale found schedule and cost prohibitive

Options to accelerate development evaluated:

- Small-scale pump built and tested successfully

- Semi-scale pump program selected, approx. 1/15th scale

- Design and SOA SLM manufacture undertaken

DOE C & CBTL Workshop 17

CFT Semi-scale Rig in Test

SLM Tiles and Outlet

DOE C & CBTL Workshop 18

CFT Semi-scale Initial Testing

Initial Tile-sidewall Leakage Addressed by Side Seals and Vacuum Clearing Ports

DOE C & CBTL Workshop 19

CFT Semi-scale Initial Test Results

• Reliable coal flow into pump by active hopper confirmed at semi-scale

• Coal lock-up in active pump duct confirmed

• Consolidated and repeatable coal plug in outlet confirmed

• Drive system modification in work to allow low-speed track operation

• Second generation SLM tiles to improve seal performance in manufacture

• Additional SLM scraper configurations in manufacture

- SLM allows low-cost manufacture of complex components quickly

• Data acquisition system sensor mod’s for lower than expected loads

• Commencing pressure testing (150 PSI max) shortly

DOE C & CBTL Workshop 20

Turning Raw Technology

into Practical Solutions

[email protected]

www.gastechnology.org @gastechnology