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MCE Deepwater Development 2016 PAU, FRANCE • 5-7 APRIL 2016 Decommissioning Subsea Abrasive Water Jet Cutting Case Study Paul Yeats Oceaneering

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Page 1: Decommissioning Subsea Abrasive Water Jet Cutting Case Studymcedd.com/wp-content/uploads/03_Paul Yeats - Oceaneering... · 2017-05-18 · Subsea Abrasive Water Jet Cutting Case Study

MCE Deepwater Development 2016

PAU, FRANCE • 5-7 APRIL 2016

Decommissioning

Subsea Abrasive Water Jet Cutting

Case Study

Paul Yeats

Oceaneering

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MCE Deepwater Development 2016

Project Description

• Multi Operators approached Oceaneering to review well schematics of 8 subsea

wells in UKCS and propose a solution for the safe and efficient recovery.

• Upon review of information for each well, each recovery would face its own

challenge (access / Non H4 profile / Cement Patio’s / unknowns – lack of cement in

annulus etc).

• Oceaneering proposed a methodology for each well including contingency options

for each.

• Project took place October/November 2015.

• Customer also indicated that pricing was to be submitted as a lump sum campaign.

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MCE Deepwater Development 2016

Primary Equipment: Internal Multi-string Cutting Tool (IMCT)

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MCE Deepwater Development 2016

Challenging Wells

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MCE Deepwater Development 2016

Cement Patio Break Up Tools

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MCE Deepwater Development 2016

Challenges: Lack of Cement in Annulus

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MCE Deepwater Development 2016

Challenges: Recovery/Non H4

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MCE Deepwater Development 2016

Dredging for Access

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MCE Deepwater Development 2016

Pile Dredging

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MCE Deepwater Development 2016

External Wellhead Cutting

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MCE Deepwater Development 2016

Wellhead Recovery

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MCE Deepwater Development 2016

Wellhead Protection Structure

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MCE Deepwater Development 2016

Recovered Structure

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MCE Deepwater Development 2016

• Through the extensive time spent up-front prior to mobilisation, we were able to

ensure the correct equipment including all contingency equipment was onboard

to cover all eventualities.

• With the correct equipment onboard, we were able to complete these 8

challenging wells within budget, on time (1 day on WOW) and without any

requirement to sail to port for further equipment mobilisations.

• Successful completion of this project using this pricing strategy shows a step

change in how these work scopes can be completed and favour all parties.

• Currently bidding further work for client based on success of operation.

Conclusion

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MCE Deepwater Development 2016

Day Rate v Lump Sum:

• High amount of wells to be Decommissioned in the UKCS – next 5 years account for

large % of decommissioning activity.

• Decommissioning is here and now.

• Risk v Reward.

• Is it feasible to bid the final (or other) stages of decommissioning on a lump sum basis?

• Do you fully know & understand your risk?

• Known knowns, known unknowns, unknown unknowns.

• Weather Risk – W.O.W

Driving Efficiencies in Decommissioning