case study setting time reduction
TRANSCRIPT
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8/7/2019 CASE STUDY SETTING TIME REDUCTION
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CELL I - Set Up Time Reduction - ( Loss Number 2 )
Product : Wheel Cylinder Machining
Approach:
Cross functional team formed
VTR Study conducted
Activities Classified as Removal, Fixing
& adjustments
Counter Measures & Kaizens Identified
Target set - 2 Months
Operation : Fine Reaming & Rolling
Machines : REAMING 2
Brakes India LimitedBrakes India Limited, Padi, Padi
Theme : Set Up Time Reduction
Back Ground : -
12 Product Varieties are Handled in Reaming Machine -2.
Customers require weekly delivery schedule than monthly delivery.
Capacity constraint is there to accommodate all the varieties by weeklyFrom pareto, we found setting time increased due to high frequency
PARETO CHART ON LOSS HOURS IN REAMIING 2
8.2
1.8
0.24 0.2
78.54
95.7910098.08
0
2
4
6
8
10
SETTING TOOL CHANGE ADJUSTMENT
LOSS
BREAK DOWN
TIMEINHRS
0
10
20
30
40
50
60
70
80
90
100
PERCENTAG
5
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Identify Machine
Set Theme
Brakes India LimitedBrakes India Limited, Padi, Padi
Conduct Time Study, Video Study
Categorize Activities Removal,Fixing & Adjustments.
Implement Kaizens for Tool Presetting
Fixture Presetting etc.,
Implement Kaizens for Conversion from
Internal to External activities
Implement Kaizens for
Internal & Adj. Activities
Sustain
Standardise
Horizontal Deployment Savings Evaluation
Identify
KAIZENS
Identify
KAIZENS
Observe Performance
SET UP TIME REDUCTION
METHODOLOGY
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Brakes India LimitedBrakes India Limited, Padi, Padi
Exist ing Target
1 Removal of Acrylic Guard Spindle To Aviod Oil Spillage Required - 5 5
23 Nos Alen screw loosening from Top
locatorFixture For holding Top locator Required - 30 30
33 Nos Alen screw removal from Top
locatorFixture To change the Part No Eliminate
Elongated radial Slot to be Provideded in
Top locator65 0
4 Grub screw loosining from spindle Spindle For holding the spindle Required - 15 15
5 Reamer & Locator removal Fixture & Spindle To change the Part No Reduce PLC to be modified 35 15
6 Bottom locator removal Fixture To change the Part No Required - 10 10
7 Washing exsisting Locators Kerosine Tank To remove the burr Required - 10 10
8 Removing Rolling tool Rolling m/c To change the Part No Required 60 60
Fixing Activity
9 Washing new Locators Kerosine Tank To remove Forign materieal Required - 10 10
10 Fixing Bottom Locator Fixture For holding the Part Required - 25 25
11 Fixing Top Locator Fixture For holding the Part Reduce PLC to be modified 30 10
12 Fixing Reamer Spindle For cutting the bore Reduce PLC to be modified 35 10
13 Tightning Grub screw to spindle Spindle For holding the spindle Required - 12 12
14 3 Nos Alen screw fixing to Top locator Fixture For holding Top locator EliminateElongated radial Slot to be Provideded in
Top locator65 0
15 Tightning 3 nos alen screw to top locator Fixture For holding Top locator Required - 25 25
16 Fixing Acrylic Guard Spindle To Aviod Oil Spillage Required - 5 5
17 Fixing Rolling tool Rolling m/cTo meet the Specification of
the ProductRequired - 25 25
Adjustment Activity
18 Bottom Dog Loosining Limit Switch To change the Part No Required - 5 5
19 Bottom Dog Adjustment Limit Switch To change the Part No setting Reduce Setting Block to be introduced 15 5
20 Bottom Dog Tightning Limit Switch For holding the Dog Required - 5 5
21 Slide Postioning slide ways For travel of reamer Eliminate Setting Block to be introduced 60 0
22 Approch Dog Loosining Limit Switch To change the Part No Required - 5 5
23 Approch Dog Adjustment Limit Switch To change the Part No setting Reduce Setting Block to be introduced 15 524 Approch Dog Tightning Limit Switch For holding the Dog Required - 5 5
25 Slide Postioning slide ways For travel of reamer Reduce Setting Block to be introduced 25 10
26 Adjustment Rolling tool Rolling m/cTo meet the Specification of
the ProductEliminate Pre setting to be Introduced 240 0
Internal Activity
27Control Plan,Drawing,Locators,&
Reamer taken from StoreTool Store To change the Part No Eliminate
Before Setting all tools lying in near the
Machine300 0
28 Mercer Plug taken from store Tool Store To change the Part No EliminateBefore Setting all tools lying in near the
Machine150 0
29 Adjustment of Mercer Plug Setting Gauge Stand To meet Master Value Reduce Pre Setting to be Introduced 80 20
30Bore Concentricity checking at S urface
TableInspection Table To Meet Product Specification Reduce K ept in Near the Machine 90 30
31Bore Surface Finish checking at
Stds.RoomInspection Table To Meet Product Specification Reduce Kept in Near the Machine 120 60
32 First off Report Preparation Inspection Table o preparation of Product History Reduce Kept in Near the Machine 180 120
Total in Seconds 1757.00 537
Total in Minutes 29.28 8.95
Time Taken (Secs)
Removing Activities
Machine : Reaming 2
Activities Split Up
Action Plan ( How )Counter
MeasureWhyWhereSl.No Activities
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Gantt Chart
AFTER - 8.95 MintsBEFORE 29.28
1 2 3 4 5 6 7 8
10 11 12 13 14 15 16 17 18 1
20 21 22 23 24 25 26 27 28 2
30
REMOVING
21
1
1
1
2
1
1
0.3
11
ADJUSTMENT
2
1
2
3
Internal
5
2
1
0.2
2
0.3
2
1 3
2
3 Remove Rolling Tool
1 Remove Locators
2 Remove Reamer
Fixing Rolling tool
5 Fixing Locators
6 Fixing Reamer
14
Control
Plan,Drawing,Locators,&
Reamer taken from Store
15 Mercer Plug taken fromstore
16Adjustment of Mercer
Plug Setting
17
Bore Concentricity
checking at Surface
Table
18Bore Surface Finish
checking at Stds.Room
1 First off Report
Preparation
Activities
13
Time In MINS
FIXING
Adjustment Rolling tool
11 Approch Dog Adjustment
Bottom Dog Adjustment
7
Elongated Slot
Introduced
PLC panel
Setting
Block
Introduced
Pre Setting
Introduced
Before Setting all tools
lying in near the Machine
Kept in Near the Machine
Brakes India LimitedBrakes India Limited, Padi, Padi
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Major ImprovementsAfterBefore
PLC Control has been changed in Electrical Panel
Elongated Slot has been changed in Top locator
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Setting Block has been Introduced
Major ImprovementsBefore After
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GROUP A GROUP B GROUP C GROUP - D
Brakes India LimitedBrakes India Limited, Padi, Padi
Machine : Reaming - 2
Part No Over all Length Reamer No Reamer length
2966 3388 / 89 58.2 / 57.8 22RS2099 170
2966 6449 58.2 / 57.8 22RS2098 170
2966 6136 / 37 58.2 / 57.8 22RS2101 170
2966 5877 59.0 / 58.5 22RS2052 160
2966 5073 59.0 / 58.5 22RS2065 170
2966 5084 59.8 / 60.3 22RS2052 160
2966 5089 59.8 / 60.3 22RS2065 170
2966 4765 63.7 / 63.2 22RS2033 170
2966 2540 52.0 / 51.6 22RS2100 150
2966 5632 55.3 / 54.8 22RS2081 150
2966 5744 55.3 / 54.8 22RS2099 170
Group C 2966 2800 90.9 / 90.4 22RS2058 190
6467 5317 79.1 / 79.7 22RS2033 170
2966 5518 79.1 / 79.7 22RS2057 190Group D
Group A
Group B
Grouping Details For Setting Block
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Results
Brakes India LimitedBrakes India Limited, Padi, Padi
A C T IV I T IE S S P IL T U P IN S E T T IN G - R E A M IN G 2
7 . 5
2 . 42
0 . 7
3 . 8 63 . 8 3
0
1 0
R E M O V I N G F I X I N G A D J U S T M E N T
NUM
BER
O
F
AC
G O O D
ACTIVITIES IN SETTING - REAMING 2
18
36
0
10
20
30
40
Bef ore A f ter
NU
MBER
II
IE
BEFORE AFTER
GOOD
EX T E R N AL AC T I IT IES
6
00
2
4
6
8
INTERA NA L EXTERNA L
N
UM
BERO
FA
CTI
I
BEFO RE A FT ER
G O O D
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Brakes India LimitedBrakes India Limited, Padi, Padi
Results
INVENTORY REDUCED
2300
7000
0
2000
4000
6000
8000
BEFORE AFTER
QTY.
BEFORE AFTER
GOOD
FREQUENCY INCREASED
BEFORE AFTER
Nos
BEFORE AFTER
GOOD
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Results
Benefits : Set Up Time Per Set Up Reduced from 30 to 9 Mins.
Brakes India LimitedBrakes India Limited, Padi, Padi
I I
9
30
0
5
10
15
20
25
30
35
May '05 June '05 July '05 Aug '05 Sep '05 Oct '05
I
I
I
Before
After
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PERFORMANCE TREND CHART
0
20
40
60
80
100
PERFORMANCE
PE
FO
MANCE 81.2 96.6 92.9 92.8 90.3 87.3 89.8 88.9 91
200 200 200 Apr- Ma Jun-Jul- Au Se
QUALITY RATE TREND
99.7
99.75
99.8
99.85
99.9
99.95
100
QUALITY
RATE
QUALITY 99.8 99.95 99.91 99.96 99.92 99.91 99.92 99.98 99.98
2002 2003 2004 Apr- M ay- Jun- Jul- Aug- Sep-
AVAILABIL I
74
76
78
80
82
84
86
88
AVAILABILI
%
AVAIL. 80.63 84.81 78.25 82.02 82.3 82.85 83.1 85 85.9
2002 2003 2004 Apr- May- Jun- Jul- Aug- Sep-
Brakes India LimitedBrakes India Limited, Padi, Padi
55
60
65
70
75
80
OEE
OEE 65. 49 70. 3 72. 61 74. 3 74. 6 72. 21 7 4. 56 76 78
2002 2003 2004 A
May
J
J
l
05 A
Se