8d corrective action report rev no. : 03 page no. 1 of 2
TRANSCRIPT
8D CORRECTIVE ACTION REPORT
Format no. : F-MRO-008
Rev no. : 03
Page No. 1 of 2
Ref. No.: Date: 05.06.2020
Customer Voice / Reported defect: VE8100 Door assly sealant crack & hemming open
Safety Failure rate high Post Cut off Fit/ Functional Aesthetic
D1: Team formation The Problem Solving Investigator, uses a multi-person approach to collect information from those directly associated with and/or impacted by the problem.
Team Leader: Aswin Kumar
Team Member Department Team Member Department
Dilip Rathore Manufacturing Sanket Chalmela Manufacturing
Girish Ranjan Kumar Product design Arun Jingound QA
Praveen Rathore Maintenance Sachin kumar Store
Piyush Gour SQA Atul Sinhal ME
D2: Describe the Problem Understand/Record the customer complaint, conversion into technical statement, Collect the data from those involved with the problem and produce a Well Formed inference. [5W1H, Histogram, 5G(Go to the spot, Examine object, Check
facts & figure, Refer to the theory, Follow operating std ) process flow chart, process map, customer complaint, problem statement, failure data, Data Inference ] D2.1 5W1H:-
5W1H Description Observation
What 1.Describe the problem in detail in
comparison with the OK part /
assembly/ operation/functioning
2. What is the effect of the
problem
1.Door assly sealant crack near lower hinge (LH &
RH) and during opening inner panel comes out of
hemming area ( Poor holding)
2. Door structure will disturb.
When
When did the problem occur?
Date: Time:_____ Ordinary Sequence During rework
maintenance Initial / shift end Online
Assly Testing Other _as per rework
100% problem
Where Where did you see the problem?
( Location / station)
WhatsApp Video 2020-06-02 at 5.12.24 PM.mp4 ( Field failure clip)
In model VE8100 both Door assly LH & RH near lower
hinge
Location: KNR, Telangana WhatsApp Video 2020-06-03 at 15.49.40.mp4 (Line observation clip)
Model: Pro 8031XM Hybrid
Sealant crack near lower hinge Sealant crack near lower hinge
8D CORRECTIVE ACTION REPORT
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Rev no. : 03
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which Which trend (pattern) did you
see the problem? ( Monthly
trend/model/application/Dealer
All over INDIA, every month as per Service
Failed vehicle details:-
S. No
Chassis No Hrs Kms
S. No Chassis No Hrs Kms
1 MC2Y3LRC0LB000932 425 7422 6 MC2Y3LRC0LC000973 265 4173
2 MC2Y3LRC0LB000937 297 4740 7 MC2Y3LRC0LC000971 135 1721
3 MC2Y3LRC0LB000945 231 3198 8 MC2Y3LRC0LB000904 294 4112
4 MC2Y3LRC0LC000970 380 6745 9 MC2Y3LRC0LB000923 308 4592
5 MC2Y3LRC0LC000972 195 2884 10 MC2Y3LRC0LB000943 294 4543
Who Is the problem related to skill?
No
How 1. How the incident happened.
During door opening driver observed sealant crack & door
part moving near lower hinge of Both LH & RH door
assembly.
D3: Implement & verify containment Implement containment to control the situation and mitigate further negative effects of the problem. (Check sheet, Rework, Segregation, Visual check 100%, testing etc ) D3.1Interim action guide line video for field:-
VID_20200604_1246
10.mp4
Upper hinge area spot details Lower hinge area spot details
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D3.2Interim action validation report ( Not defined in drg )
Hemming flange clamping force report in Kgf
Side Precondition After brazing Remarks
LH 14 10 >33 >33 No deformation
RH 9 9 >34 >35 No deformation Note:- Above test concluded that Door assembly will sustain the door opening force & further RIG validation is planned by PDD
D3.4Interim action validation report
Location Material Sorted Quantities/Comments Resp Target Remarks
Customer Dealer: YES NO 10set of door dispatched DR 29/06/20 Dully brazed
Dealer YES NO Guideline attached AK 15/06/2020
Transit vehicle YES NO NIL
Stock yard YES NO 15 vehicle identified & rework under process
DR 17/06/2020
In house YES NO Checked & Brazing started
from plant
DR 06/06/2020 Started
Ware house YES NO NIL
Supplier YES NO NIL
D4: Root Cause Analysis Identify the Possible Causes of the problem for both occurrence and non-detection. Conduct a Root Cause Analysis to determine true Root Cause (Brain Storming session, C & E diag, FTA, Why-Why Analysis, process map, etc)
D4.1: Cause and Effect diagram:-
8D CORRECTIVE ACTION REPORT
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Rev no. : 03
Page No. 4 of 2
D4.2: Model wise comparison report:-
Model wise outer to inner gap comparison report
Sr no Insp. Point
Pro3000/6000 Pro2000 Pro8000
Remarks
LH RH LH RH LH RH
Outer to Inner gap 1.5±1.5
Outer to Inner 1.5±1.5
Outer to Inner gap 1.9±1.5
Outer to Inner gap 1.9 ±1.5
Outer to Inner gap 2.07 ±1.5
Outer to Inner gap 2.07 ±1.5
1 Upper hinge
2.5 2 2 3 3.5 3.2 In pro8000 gap is higher side
2 Lower hinge
2.5 2 2 3.1 3.4 3.0
Model wise outer flange height comparison report
S no Insp. Point
Pro3000/6000 Pro2000 Pro8000
Remarks
LH RH LH RH LH RH
Outer flange Height
Outer flange Height
Outer flange Height
Outer flange Height
Outer flange Height 8.0± 1.0
Outer flange Height 8.0± 1.0
1 Upper hinge
11 11 11.5 11 7.8 7.9 As per drg OK in Pro8000 height observed lesser than other models
2 Lower hinge
11 11.5 12 11.5 8 7.8
Model wise Hemming thickness comparison report
S.NO. Insp. Point
Pro3000/6000 Pro2000 Pro8000
Remarks
LH RH LH RH LH RH
Hemming thickness 2.8+0.1
Hemming thickness 2.8+0.1
Hemming thickness 2.4+0.1
Hemming thickness 2.4+0.1
Hemming thickness 2.54+0.1
Hemming thickness 2.54+0.1
1 Upper hinge
3 3.0 2.44 2.46 2.7 2.9
Pro8000 & Pro3000 thickness more &
Pro1900 is OK 2
Lower hinge
3.05 2.96 2.4 2.44 2.6 2.7
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Page No. 5 of 2
D4.2: Hemming overlap report (Total 5 reading taken )
Note:- 0.5 overlap @ LH12 problematic area against 1~3mm (calculated value)
Note:- 1.2 overlap @ RH12 problematic area against 1~3 (calculated value)
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D4.4: Door hemming thickness report(Total 5 reading taken).
Note:- LH side OK & RH side Hemming thickness is more by 0.1mm in some door mentioned area
4.5: Possible cause verification report.
S.no Variable Parameters Spec. Actual Status
1 Man
Unskilled operator Skill (L2-L4) L3 OK
Operator fatigue Visual OK OK
Wrong model run Not possible separate
line L3 OK
2 Machine
Clamping working condition Rigid clamping Found Ok OK
Bed surface waviness No deep marks Found OK OK
Inner locator worn out no step Found OK OK
Vacuum pads not effective Should be effective Found OK OK
Roller worn out no step Found OK OK
3 Method
Locator position not Ok Gap as per Design OK OK
Program disturbed Check visual OK OK
Heming flange overlap –LH 1.0~6.0mm 0.5~3.6mm OK
Heming flange overlap –RH 1.0~6.0mm 0.4~3.5mm OK
Heming thickness more –LH 2.54+0.1mm 2.65~2.7mm NOK
Heming thickness more – RH 2.54+0.1mm 2.7~2.9mm NOK
Door outer to inner gap more-LH 2.07+/-1.5mm 2.8~3.6mm OK
Door outer to inner gap more-RH 2.07+/-1.5mm 2.9~3.4mm OK
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Page No. 7 of 2
Hemming bed outer locator LH 36 / 35.2 (-0.05/-0.1)mm 35.94/35.15mm OK
Hemming bed outer locator RH 36 / 35.4 (-0.05/-0.1)mm 35.94/35.35mm OK
Hemming bed inner locator LH 20(-0.05/-0.1)mm 19.96mm OK
Hemming bed inner locator LH 25(-0.05/-0.1)mm 24.95mm OK
Hemming bed inner locator RH 20(-0.05/-0.1)mm 19.95mm OK
Hemming bed inner locator RH 25(-0.05/-0.1)mm 24.95mm OK
Expired sealant As per mentioned As per
revalidated certificate OK
OK
Sealant qty less in Diameter 3.0mm 2.0mm OK
Sealant position not ok 5~6mm 02.0mm NOK
Program changed History No history OK
4 Material
Inner thickness LH 0.8mm 0.83mm OK
Outer thickness-RH 0.85mm 0.87mm OK
Inner thickness –LH 0.8mm 0.83mm OK
Outer thickness-RH 0.85mm 0.87mm OK
Door out flange height less-LH 8+1.0/-0.5mm 7.5~8mm OK
Door out flange height less-RH 8+1.0/-0.5mm 7.5~8mm OK
Inner flange wrinkles Wrinkle free Not Ok NOK
Outer flange wrinkles Wrinkle free Not Ok NOK
Flange height under size As per drg 7.4~8.0mm OK
4 Design Lower hinge stress area overlap less
1~3.0mm (value is similar in all model at same section)
Not ok NOK
Door tilting instruction missing Sticker Available OK
D4.6:Sealant Expiry study report
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D4.7: Sealant missing:-
Note:- Sealant dispensing done manually.
D4.8:Door panel inspection report
Door panel thickness inspection report
Sr no LH RH
Remarks Inner(spec 0.80) Outer(Spec0.85) Inner(spec 0.80) Outer(Spec0.85)
1 0.83/0.89 0.86/0.83 0.84/0.88 0.85/0.84
2 0.84 0.85/0.88 0.85/0.88 0.83/0.83
3 0.85 0.84 0.82/0.86 0.84
4 0.85 0.85/0.87 0.82/0.9 0.84
Avg 0.85 0.85 0.85 0.84
Hemming spec 2.54 2.54
Note:- At flange area heavy burr get folded found, wrinkle coming thickness variation from 0.83~1.7mm observed
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D4.9: Conclusion
Conclusion:- 1. Hemming thickness at hinge area 2.8mm against 2.54+0.1
2. Hemming overlap 0.5~1.2 mm observed against 1.0~3.0. 3. Hemming sealant position 0~2mm against 5~6mm.
D5: Develop Permanent Corrective actions Develop Permanent Solution(s) that address each Root Cause. Verify and test the Permanent Solution(s).
Defects phenomenon
Possible Root Causes
Action plan / Activity plan Dept. Resp Target date Status
Door hemming flange opening
during door assembly opening
Hemming thickness more
Robot program to be optimized Maintenance
PB 10/06/2020 G
Daily sample inspection to be started for Hemming thickness @ PDI
Mfg. SC 15/06/2020 G
Door hemming thickness spec tolerance to be increased after trial of new door inner from JBM
1. Hinge area2.54+0.2 2. Other area 2.54+0.3
PDD/QA GKR/ AAJ
15/07/2020 Y
Door overlap lower side
Door inner locally developed trial to be taken & Explore possibility of overlap increase
PDD/Mat/Mfg
GKR/ DK/SC
15/07/2020 Y
Brazing 7 spots started from line . SOP to be displayed near station Cut off no is A0000381
Mfg. SC 15/06/2020 G
With & without brazing door assembly to be provided for validation
Mfg SC 24/06/2020 G
With Brazing & without brazing RIG validation to be done
PDD GKR W2034 Y
After validation Drg to be updated
PDD GKR W2035 Y
Sealant qty less / missing
Sealant dispensing area to be ensured during sealant assembly SOP to be displayed near station
Mfg. SC 15/06/2020 G
Sealant position not Ok, manual application
Template to be provided ME AS 10/07/2020 Y
Door inner wrinkles
Local part to be implemented Purchase DK 30/07/2020 Y
8D CORRECTIVE ACTION REPORT
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D5.2: Door hemming thickness report:-
.
Note:-
1. Hemming flange opening force with 2.7thickness, force is 20 kgf & with 2.55mm hemming thickness improved flange opening force till 28kgf.
2. Line mark observed in door outer side after hemming thickness of 2.55mm. Need to validate for line mark after painting if not OK, we will readjust to 2.7mm
3. Overal thickness is coming up to 2.9mm reason may be due to panel folded bur, wrinkles dust etc.
After set lower side-LH
Before Upper side-LH
After set lower side-RH
Before set Higher side-RH
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D5.3: Hemming overlap optimization report:-
Note:- 1.2mm overlap increased in problematic area
Note:- No major improvement
6: Validate Permanent Corrective Actions Validate that the chosen solution is effective [CAE, Validation, performance, Customer feedback]
D6.1: Door flange opening force before & after in kgf
After set -LH Before -LH
1.2mm
After set -LH Before -LH
1.2mm
0.4mm
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Hemming flange clamping force report in Kgf
Side Precondition hemming ht correction After brazing Remarks
LH 14 10 28 29 >33 >33 No deformation
RH 9 9 29 28 >34 >35 No deformation
D6.2 Brazing trial Slam test report awaited:-
D7: Prevent Recurrence Prevent recurrence of the problem at the problem site and across the organization
Related Document Updates Yes No Not
applicable Resp. Target
PFMEA Yes CFT 30/06/2020
PPAP
Poka yoke Sheet
Drawing
One point lesson
Process Flow
SOP Update Yes SC 20/07/2020
Control plan Yes AAJ 20/07/2020
Process Audit Sheet
Central Quality Audit Sheet
Quality Gate Check Sheet Yes SC 13/06/2020
Field Vehicle Resolution Reactive Proactive Selective
Address similar system horizontal Deployment Sr
no
Process /product item Resp Target status
1 Pro1000,Pro3000/6000 brazing implemented other than Pro2000
SC Already done
Green
2 Brazing to be added in the drg for above models
GKR W2036 Y
8D CORRECTIVE ACTION REPORT
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Page No. 13 of 2
Model wise Hemming thickness comparison report
S.NO. Insp. Point
Pro3000/6000 Pro2000
Remarks LH RH LH RH
Hemming thickness spec(2.8+0.1)
Hemming thickness spec(2.8+0.1)
Hemming thickness spec(2.4+0.1)
Hemming thickness spec(2.4+0.1)
1 Upper hinge 2.85 2.84 2.44 2.46 All model ensured hemming thickness at lower side
2 Lower hinge 2.85 2.8 2.4 2.44
Conclusion:- Pro3000/6000 hemming thickness set ( no gap between outer to inner) @
lower side & flange deformation still observed. also heavy line mark is coming So set the
hemming thickness at higher side & brazing required to come out of the issue.
D8: recognize contributions